Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-04-22 — TX
Operator
Shell Pipeline Co., L.p.
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$500
Incident datetime
2014-04-22 11:00
Report number
Location
TX
Narrative
A one inch threaded auxilary drain pipe was found to have cracked threads at the elbow connection. This section of the drain line was inactive. The one inch piping was removed and plugged at the connection to the two inch drain line.
Detailed record list
Report Received Date
2014-05-15 00:00:00
Iyear
2014
Report Number
20140189
Supplemental Number
19487
Report Type
Supplemental Final
Operator Id
31174
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2014-04-22 11:00:00
Location Latitude
29.9006722
Location Longitude
-94.0055528
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
3
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-04-22 11:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The System Was Not Running At The Time Of Discovery.
On Site Datetime
2014-04-22 11:00:00
Nrc Rpt Datetime
2014-04-22 12:04:00
Nrc Rpt Num
1080474
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pt. Arthur Products Station
Segment Name
Paps #4 Booster
Onshore State Abbreviation
Tx
Onshore Postal Code
77640
Onshore City Name
Port Arthur
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Auxilary Drain Piping Threaded Elbow
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
500
Est Cost Emergency
19500
Est Cost Environmental
0
Est Cost Other
0
Prpty
20000
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Preparer Name
R****** K*****
Preparer Title
Regulatory Specialist
Preparer Email
R*************@s****.com
Preparer Telephone
713 241 1064
Prepared Date
2014-06-19 00:00:00
Authorizer Name
B**** S*******
Authorizer Telephone
713 241 3620
Authorizer Title
Integrity And Regulatory Services Manager
Authorizer Email
B*************@s****.com
Narrative
A one inch threaded auxilary drain pipe was found to have cracked threads at the elbow connection. This section of the drain line was inactive. The one inch piping was removed and plugged at the connection to the two inch drain line.
| Report Received Date | 2014-05-15 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140189 |
| Supplemental Number | 19487 |
| Report Type | Supplemental Final |
| Operator Id | 31174 PHMSA Enforcement |
| Name | Shell Pipeline Co., L.p. |
| Operator Street Address | 150 North Dairy Ashford Road Wck Bldg. A |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77079 |
| Local Datetime | 2014-04-22 11:00:00 |
| Location Latitude | 29.9006722 Google Maps OpenStreetMap |
| Location Longitude | -94.0055528 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 3 |
| Recovered Bbls | 3 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2014-04-22 11:00:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | The System Was Not Running At The Time Of Discovery. |
| On Site Datetime | 2014-04-22 11:00:00 |
| Nrc Rpt Datetime | 2014-04-22 12:04:00 |
| Nrc Rpt Num | 1080474 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Pt. Arthur Products Station |
| Segment Name | Paps #4 Booster |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77640 |
| Onshore City Name | Port Arthur |
| Onshore County Name | Jefferson |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Pipe Facility Type | Interstate |
| Item Involved | Other |
| Item Involved Details | Auxilary Drain Piping Threaded Elbow |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 500 |
| Est Cost Emergency | 19500 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 20000 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Threaded Connection/coupling Failure |
| Eq Failure Type | Threaded Connection/coupling Failure |
| Preparer Name | R****** K***** |
| Preparer Title | Regulatory Specialist |
| Preparer Email | R*************@s****.com |
| Preparer Telephone | 713 241 1064 |
| Prepared Date | 2014-06-19 00:00:00 |
| Authorizer Name | B**** S******* |
| Authorizer Telephone | 713 241 3620 |
| Authorizer Title | Integrity And Regulatory Services Manager |
| Authorizer Email | B*************@s****.com |
| Narrative | A one inch threaded auxilary drain pipe was found to have cracked threads at the elbow connection. This section of the drain line was inactive. The one inch piping was removed and plugged at the connection to the two inch drain line. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA