HL incident on 2014-04-14 — TX

Operator
Plains Pipeline, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$26,500
Incident datetime
2014-04-14 15:24
Report number
Location
TX
Narrative
Approximately 500 bbls of crude oil were released as a result of failed coupling on the booster pump. The coupling on the booster pump came apart, which dropped the shaft and opened the seal, causing oil to release. Operators, along with the control center, rerouted the flow to stop the leak. The motor was verified to be in proper working order, however, the pump was replaced.The national response center (nrc) was notified. Nrc assigned report number 1079834. Supplemental narrative: after further review, part g6 has been updated from pump or pump-related equipment to threaded connection/coupling failure, along with the addition of the sub-cause over torqueing in g6-other, to better clarify the failure. As of 11/15/2016, part d, number 8 has been revised as the costs were originally input incorrectly.
Detailed record list
Report Received Date
2014-05-14 00:00:00
Iyear
2014
Report Number
20140187
Supplemental Number
21839
Report Type
Supplemental Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-04-14 15:24:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
500
Recovered Bbls
500
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-04-14 15:24:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-04-14 15:25:00
Restart Datetime
2014-04-14 15:55:00
On Site Datetime
2014-04-14 15:50:00
Nrc Rpt Datetime
2014-04-15 15:10:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Jal Basin Station
Segment Name
Jal Basin Station
Onshore State Abbreviation
Nm
Onshore Postal Code
88252
Onshore City Name
Jal
Onshore County Name
Lea
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
1947
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
11000
Est Cost Prop Damage
26500
Est Cost Emergency
87531
Est Cost Environmental
40000
Est Cost Other
0
Prpty
165031
Accident Psig
43
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Mechanical Coupling
Eq Additional Other Ind
Yes
Eq Additional Other Details
Over Torqueing
Preparer Name
C******* C*****
Preparer Title
Compliance Specialist
Preparer Email
C*******@p****.com
Preparer Telephone
713-993-5080
Preparer Fax
713-646-4310
Prepared Date
2016-11-15 00:00:00
Authorizer Name
T***** M*****
Authorizer Telephone
713-646-4109
Authorizer Title
Sr Dir Of Environmental And Regulatory Compliance
Authorizer Email
T*******@p****.com
Narrative
Approximately 500 bbls of crude oil were released as a result of failed coupling on the booster pump. The coupling on the booster pump came apart, which dropped the shaft and opened the seal, causing oil to release. Operators, along with the control center, rerouted the flow to stop the leak. The motor was verified to be in proper working order, however, the pump was replaced.The national response center (nrc) was notified. Nrc assigned report number 1079834. Supplemental narrative: after further review, part g6 has been updated from pump or pump-related equipment to threaded connection/coupling failure, along with the addition of the sub-cause over torqueing in g6-other, to better clarify the failure. As of 11/15/2016, part d, number 8 has been revised as the costs were originally input incorrectly.
Report Received Date 2014-05-14 00:00:00
Iyear 2014
Report Number 20140187
Supplemental Number 21839
Report Type Supplemental Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-04-14 15:24:00
Location Latitude 32.080668 Google Maps OpenStreetMap
Location Longitude -103.178983 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 500
Recovered Bbls 500
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-04-14 15:24:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-04-14 15:25:00
Restart Datetime 2014-04-14 15:55:00
On Site Datetime 2014-04-14 15:50:00
Nrc Rpt Datetime 2014-04-15 15:10:00
Nrc Rpt Num 1079834 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Jal Basin Station
Segment Name Jal Basin Station
Onshore State Abbreviation Nm
Onshore Postal Code 88252
Onshore City Name Jal
Onshore County Name Lea
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 1947
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 11000
Est Cost Prop Damage 26500
Est Cost Emergency 87531
Est Cost Environmental 40000
Est Cost Other 0
Prpty 165031
Accident Psig 43
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Mechanical Coupling
Eq Additional Other Ind Yes
Eq Additional Other Details Over Torqueing
Preparer Name C******* C*****
Preparer Title Compliance Specialist
Preparer Email C*******@p****.com
Preparer Telephone 713-993-5080
Preparer Fax 713-646-4310
Prepared Date 2016-11-15 00:00:00
Authorizer Name T***** M*****
Authorizer Telephone 713-646-4109
Authorizer Title Sr Dir Of Environmental And Regulatory Compliance
Authorizer Email T*******@p****.com
Narrative Approximately 500 bbls of crude oil were released as a result of failed coupling on the booster pump. The coupling on the booster pump came apart, which dropped the shaft and opened the seal, causing oil to release. Operators, along with the control center, rerouted the flow to stop the leak. The motor was verified to be in proper working order, however, the pump was replaced.The national response center (nrc) was notified. Nrc assigned report number 1079834. Supplemental narrative: after further review, part g6 has been updated from pump or pump-related equipment to threaded connection/coupling failure, along with the addition of the sub-cause over torqueing in g6-other, to better clarify the failure. As of 11/15/2016, part d, number 8 has been revised as the costs were originally input incorrectly.

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