HL incident on 2014-04-14 — PA

Operator
Kiantone Pipeline Corp
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$122,000
Incident datetime
2014-04-14 08:30
Report number
Location
PA
Narrative
At 8:30am on april 14, 2014, company personnel discovered crude oil stained grass in kiantone's pipeline right-of-way during a pipeline valve exercise. Response actions were initiated immediately including isolation and drainage of the section of crude oil pipeline in the right of way (note: the line had already been shut down due to an ongoing refinery turnaround.) response equipment and personnel were mobilized and the landowner, anderson construction, was contacted. Personnel then defined the extent of the release zone and deployed precautionary boom in a nearby waterway (no product ever entered the waterway.) notifications were made to the pennsylvania department of environmental protection, the national response center and the local emergency planning committee. Excavation and soil removal revealed a pinhole corrosion anomaly on component 3 of kiantone pipeline's 12" crude oil pipeline. Coating was abated and the line was inspected. A plidco clamp was installed over the anomaly and coating restored. Additional soil was removed and disposed to an approved landfill. Total volume released was estimated to be 50-100 gallons.
Detailed record list
Report Received Date
2014-05-14 00:00:00
Iyear
2014
Report Number
20140186
Supplemental Number
19384
Report Type
Original
Operator Id
Name
Kiantone Pipeline Corp
Operator Street Address
Po Box 780
Operator City Name
Warren
Operator State Abbreviation
PA
Operator Postal Code
16365
Local Datetime
2014-04-14 08:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
1.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2014-04-14 08:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Already Shutdown Due To Refinery Turnaround
On Site Datetime
2014-04-14 08:35:00
Nrc Rpt Datetime
2014-04-14 10:02:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Kiantone Pipeline Corporation
Segment Name
12" Crude Line - Component #3
Onshore State Abbreviation
Pa
Onshore Postal Code
16365
Onshore City Name
Warren
Onshore County Name
Warren
Designated Location
Milepost/valve Station
Designated Name
168+01
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
80
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12.5
Pipe Wall Thickness
0.25
Pipe Smys
35000
Pipe Specification
Grade B
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Us Steele
Pipe Coating Type
Coal Tar
Installation Year
1971
Manufactured Year
1971
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
11000
Est Cost Gas Released
200
Est Cost Prop Damage
122000
Est Cost Emergency
98500
Est Cost Environmental
18300
Est Cost Other
0
Prpty
250000
Accident Psig
200
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
18543
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Restricted To Refinery Unit Turnaround
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Line was idle due to refinery shutdown
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1972
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2013
Close Interval Survey Year
2013
Prior Damage
Yes
Collected Data Ind
Yes
Ultrasonic Ind
Yes
Ultrasonic Recent Year
2014
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D***** S*****
Preparer Title
Regulatory Compliance Manager
Preparer Email
D********@u**.com
Preparer Telephone
8147264846
Preparer Fax
8147264798
Prepared Date
2014-05-14 00:00:00
Authorizer Name
F******** J* M***** J**
Authorizer Telephone
8147264726
Authorizer Title
Vice President Supply And Transportation
Authorizer Email
F******@u**.com
Narrative
At 8:30am on april 14, 2014, company personnel discovered crude oil stained grass in kiantone's pipeline right-of-way during a pipeline valve exercise. Response actions were initiated immediately including isolation and drainage of the section of crude oil pipeline in the right of way (note: the line had already been shut down due to an ongoing refinery turnaround.) response equipment and personnel were mobilized and the landowner, anderson construction, was contacted. Personnel then defined the extent of the release zone and deployed precautionary boom in a nearby waterway (no product ever entered the waterway.) notifications were made to the pennsylvania department of environmental protection, the national response center and the local emergency planning committee. Excavation and soil removal revealed a pinhole corrosion anomaly on component 3 of kiantone pipeline's 12" crude oil pipeline. Coating was abated and the line was inspected. A plidco clamp was installed over the anomaly and coating restored. Additional soil was removed and disposed to an approved landfill. Total volume released was estimated to be 50-100 gallons.
Report Received Date 2014-05-14 00:00:00
Iyear 2014
Report Number 20140186
Supplemental Number 19384
Report Type Original
Operator Id 10250 PHMSA Enforcement
Name Kiantone Pipeline Corp
Operator Street Address Po Box 780
Operator City Name Warren
Operator State Abbreviation PA
Operator Postal Code 16365
Local Datetime 2014-04-14 08:30:00
Location Latitude 41.831164 Google Maps OpenStreetMap
Location Longitude -79.117514 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 1.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2014-04-14 08:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Already Shutdown Due To Refinery Turnaround
On Site Datetime 2014-04-14 08:35:00
Nrc Rpt Datetime 2014-04-14 10:02:00
Nrc Rpt Num 1079694 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Kiantone Pipeline Corporation
Segment Name 12" Crude Line - Component #3
Onshore State Abbreviation Pa
Onshore Postal Code 16365
Onshore City Name Warren
Onshore County Name Warren
Designated Location Milepost/valve Station
Designated Name 168+01
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 80
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12.5
Pipe Wall Thickness 0.25
Pipe Smys 35000
Pipe Specification Grade B
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Us Steele
Pipe Coating Type Coal Tar
Installation Year 1971
Manufactured Year 1971
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 11000
Est Cost Gas Released 200
Est Cost Prop Damage 122000
Est Cost Emergency 98500
Est Cost Environmental 18300
Est Cost Other 0
Prpty 250000
Accident Psig 200
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 18543
Internal Inspection Ind Yes
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Restricted To Refinery Unit Turnaround
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Line was idle due to refinery shutdown
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1972
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2013
Close Interval Survey Year 2013
Prior Damage Yes
Collected Data Ind Yes
Ultrasonic Ind Yes
Ultrasonic Recent Year 2014
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name D***** S*****
Preparer Title Regulatory Compliance Manager
Preparer Email D********@u**.com
Preparer Telephone 8147264846
Preparer Fax 8147264798
Prepared Date 2014-05-14 00:00:00
Authorizer Name F******** J* M***** J**
Authorizer Telephone 8147264726
Authorizer Title Vice President Supply And Transportation
Authorizer Email F******@u**.com
Narrative At 8:30am on april 14, 2014, company personnel discovered crude oil stained grass in kiantone's pipeline right-of-way during a pipeline valve exercise. Response actions were initiated immediately including isolation and drainage of the section of crude oil pipeline in the right of way (note: the line had already been shut down due to an ongoing refinery turnaround.) response equipment and personnel were mobilized and the landowner, anderson construction, was contacted. Personnel then defined the extent of the release zone and deployed precautionary boom in a nearby waterway (no product ever entered the waterway.) notifications were made to the pennsylvania department of environmental protection, the national response center and the local emergency planning committee. Excavation and soil removal revealed a pinhole corrosion anomaly on component 3 of kiantone pipeline's 12" crude oil pipeline. Coating was abated and the line was inspected. A plidco clamp was installed over the anomaly and coating restored. Additional soil was removed and disposed to an approved landfill. Total volume released was estimated to be 50-100 gallons.

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