HL incident on 2014-04-11 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2014-04-11 16:15
Report number
Location
TX
Narrative
Local enterprise pipeline technician discovered a leaking pump seal at the wildfire station station at 08:45. While investigating the cause of the leak the technician discovered that the pump seal packing had failed from plunger rod wear to failure. Further review revealed that the piping to the sump was partially plugged and prevented release from being contained fully in the sump. Piping was cleaned of blockage and all sump piping was inspected for same debris blocking issues. Pump was isolated to prevent further release of crude. Pump packing was replaced and inspected. No further action was necessary. Soil remediation was performed and completed.
Detailed record list
Report Received Date
2014-05-11 00:00:00
Iyear
2014
Report Number
20140183
Supplemental Number
20008
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-04-11 08:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4.5
Recovered Bbls
4.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-04-11 16:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-04-11 18:15:00
Restart Datetime
2014-04-14 00:00:00
On Site Datetime
2014-04-14 12:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wildfire 1 Gasso Pump
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Odessa
Onshore County Name
Midland
Designated Location
Milepost/valve Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
400
Est Cost Prop Damage
1500
Est Cost Emergency
1000
Est Cost Environmental
500
Est Cost Other
0
Prpty
3400
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
S**** D****
Preparer Title
Senior Pipeline Compliance Engineer
Preparer Email
S******@e****.com
Preparer Telephone
713.381.6487
Prepared Date
2014-12-22 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713.381.6487
Authorizer Title
Senior Pipeline Compliance Engineer
Authorizer Email
S******@e****.com
Narrative
Local enterprise pipeline technician discovered a leaking pump seal at the wildfire station station at 08:45. While investigating the cause of the leak the technician discovered that the pump seal packing had failed from plunger rod wear to failure. Further review revealed that the piping to the sump was partially plugged and prevented release from being contained fully in the sump. Piping was cleaned of blockage and all sump piping was inspected for same debris blocking issues. Pump was isolated to prevent further release of crude. Pump packing was replaced and inspected. No further action was necessary. Soil remediation was performed and completed.
Report Received Date 2014-05-11 00:00:00
Iyear 2014
Report Number 20140183
Supplemental Number 20008
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-04-11 08:45:00
Location Latitude 31.718902 Google Maps OpenStreetMap
Location Longitude -102.21213 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4.5
Recovered Bbls 4.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-04-11 16:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-04-11 18:15:00
Restart Datetime 2014-04-14 00:00:00
On Site Datetime 2014-04-14 12:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wildfire 1 Gasso Pump
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Odessa
Onshore County Name Midland
Designated Location Milepost/valve Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Pump
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 400
Est Cost Prop Damage 1500
Est Cost Emergency 1000
Est Cost Environmental 500
Est Cost Other 0
Prpty 3400
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Preparer Name S**** D****
Preparer Title Senior Pipeline Compliance Engineer
Preparer Email S******@e****.com
Preparer Telephone 713.381.6487
Prepared Date 2014-12-22 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713.381.6487
Authorizer Title Senior Pipeline Compliance Engineer
Authorizer Email S******@e****.com
Narrative Local enterprise pipeline technician discovered a leaking pump seal at the wildfire station station at 08:45. While investigating the cause of the leak the technician discovered that the pump seal packing had failed from plunger rod wear to failure. Further review revealed that the piping to the sump was partially plugged and prevented release from being contained fully in the sump. Piping was cleaned of blockage and all sump piping was inspected for same debris blocking issues. Pump was isolated to prevent further release of crude. Pump packing was replaced and inspected. No further action was necessary. Soil remediation was performed and completed.

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