HL incident on 2014-04-08 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,160
Incident datetime
2014-04-08 11:44
Report number
Location
OK
Narrative
During normally scheduled mainline valve maintenance, personnel removed the incorrect plug on the valve, causing the release. The plug was replaced, maintenance was completed and the valve returned to service. Product was recovered from the valve can and reclaimed by cycling it through a sump system at the nearby magellan terminal facility. A total of 4,380 pounds of hydro-excavated mud and rock were solidified and disposed of properly as a result of the cleanup activities at this location.
Detailed record list
Report Received Date
2014-05-07 00:00:00
Iyear
2014
Report Number
20140180
Supplemental Number
19360
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2014-04-08 11:44:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
1.07
Recovered Bbls
1.07
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-04-08 11:44:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Already Down Between Shipments At The Time Of The Release
On Site Datetime
2014-04-08 11:44:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Wathena Jct. To Des Moines #7-16" Line
Segment Name
Line Id 6395
Onshore State Abbreviation
Ia
Onshore Postal Code
50125
Onshore City Name
Indianola
Onshore County Name
Warren
Designated Location
Milepost/valve Station
Designated Name
318.15
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
125
Est Cost Prop Damage
1160
Est Cost Emergency
18000
Est Cost Environmental
0
Est Cost Other
500
Est Cost Other Details
Skim Small Amounts Of Oil Off Water In Valve Can
Prpty
19785
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Preparer Name
K****** L* L******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2014-05-07 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
During normally scheduled mainline valve maintenance, personnel removed the incorrect plug on the valve, causing the release. The plug was replaced, maintenance was completed and the valve returned to service. Product was recovered from the valve can and reclaimed by cycling it through a sump system at the nearby magellan terminal facility. A total of 4,380 pounds of hydro-excavated mud and rock were solidified and disposed of properly as a result of the cleanup activities at this location.
Report Received Date 2014-05-07 00:00:00
Iyear 2014
Report Number 20140180
Supplemental Number 19360
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2014-04-08 11:44:00
Location Latitude 41.41579 Google Maps OpenStreetMap
Location Longitude -93.62086 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 1.07
Recovered Bbls 1.07
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-04-08 11:44:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Already Down Between Shipments At The Time Of The Release
On Site Datetime 2014-04-08 11:44:00
Ignite Ind No
Explode Ind No
Pipe Fac Name Wathena Jct. To Des Moines #7-16" Line
Segment Name Line Id 6395
Onshore State Abbreviation Ia
Onshore Postal Code 50125
Onshore City Name Indianola
Onshore County Name Warren
Designated Location Milepost/valve Station
Designated Name 318.15
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 125
Est Cost Prop Damage 1160
Est Cost Emergency 18000
Est Cost Environmental 0
Est Cost Other 500
Est Cost Other Details Skim Small Amounts Of Oil Off Water In Valve Can
Prpty 19785
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Preparer Name K****** L* L******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7377
Prepared Date 2014-05-07 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative During normally scheduled mainline valve maintenance, personnel removed the incorrect plug on the valve, causing the release. The plug was replaced, maintenance was completed and the valve returned to service. Product was recovered from the valve can and reclaimed by cycling it through a sump system at the nearby magellan terminal facility. A total of 4,380 pounds of hydro-excavated mud and rock were solidified and disposed of properly as a result of the cleanup activities at this location.

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