HL incident on 2014-04-08 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5
Incident datetime
2014-04-08 07:15
Report number
Location
GA
Narrative
On april 8, 2014 at 07:15 gasoline was found in an access well, surrounding gravel, and the catch basin in the tank farm 3 manifold area. Exploratory digging began immediately and the area was monitored to determine the source. On april 10, 2014 at 1300 a loose connection was found on the stem seal leak detection tubing for gasoline unit 5. The unit was shut down and the connection was replaced. Final cleanup was completed by 13:30 on april 10th.
Detailed record list
Report Received Date
2014-05-07 00:00:00
Iyear
2014
Report Number
20140179
Supplemental Number
19367
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2014-04-08 07:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.79
Recovered Bbls
0.79
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-04-08 07:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-04-10 13:00:00
Restart Datetime
2014-04-10 13:30:00
On Site Datetime
2014-04-08 07:15:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Bengal/baton Rouge
Segment Name
Baton Rouge Tankfarm #3 - Manifold
Onshore State Abbreviation
La
Onshore Postal Code
70748
Onshore City Name
Jackson
Onshore County Name
East Feliciana
Designated Location
Milepost/valve Station
Designated Name
248
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
85
Est Cost Prop Damage
5
Est Cost Emergency
24000
Est Cost Environmental
0
Est Cost Other
0
Prpty
24090
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Preparer Name
K**** M****
Preparer Title
District Compliance Coordinator
Preparer Email
K*****@c******.com
Preparer Telephone
601-765-9768
Preparer Fax
770-754-8489
Prepared Date
2014-05-09 00:00:00
Authorizer Name
A*** T*****
Authorizer Telephone
678-762-2872
Authorizer Title
Regulatory Manager
Authorizer Email
A******@c******.com
Narrative
On april 8, 2014 at 07:15 gasoline was found in an access well, surrounding gravel, and the catch basin in the tank farm 3 manifold area. Exploratory digging began immediately and the area was monitored to determine the source. On april 10, 2014 at 1300 a loose connection was found on the stem seal leak detection tubing for gasoline unit 5. The unit was shut down and the connection was replaced. Final cleanup was completed by 13:30 on april 10th.
Report Received Date 2014-05-07 00:00:00
Iyear 2014
Report Number 20140179
Supplemental Number 19367
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2014-04-08 07:15:00
Location Latitude 30.71133 Google Maps OpenStreetMap
Location Longitude -91.27589 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.79
Recovered Bbls 0.79
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-04-08 07:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-04-10 13:00:00
Restart Datetime 2014-04-10 13:30:00
On Site Datetime 2014-04-08 07:15:00
Ignite Ind No
Explode Ind No
Pipe Fac Name Bengal/baton Rouge
Segment Name Baton Rouge Tankfarm #3 - Manifold
Onshore State Abbreviation La
Onshore Postal Code 70748
Onshore City Name Jackson
Onshore County Name East Feliciana
Designated Location Milepost/valve Station
Designated Name 248
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Pipe Facility Type Interstate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Release Type Leak
Leak Type Connection Failure
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 85
Est Cost Prop Damage 5
Est Cost Emergency 24000
Est Cost Environmental 0
Est Cost Other 0
Prpty 24090
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Preparer Name K**** M****
Preparer Title District Compliance Coordinator
Preparer Email K*****@c******.com
Preparer Telephone 601-765-9768
Preparer Fax 770-754-8489
Prepared Date 2014-05-09 00:00:00
Authorizer Name A*** T*****
Authorizer Telephone 678-762-2872
Authorizer Title Regulatory Manager
Authorizer Email A******@c******.com
Narrative On april 8, 2014 at 07:15 gasoline was found in an access well, surrounding gravel, and the catch basin in the tank farm 3 manifold area. Exploratory digging began immediately and the area was monitored to determine the source. On april 10, 2014 at 1300 a loose connection was found on the stem seal leak detection tubing for gasoline unit 5. The unit was shut down and the connection was replaced. Final cleanup was completed by 13:30 on april 10th.

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