Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2014-03-28 — TX
Operator
Kinder Morgan Crude And Condensate Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$100
Incident datetime
2014-03-28 18:00
Report number
Location
TX
Narrative
On 3/28/14 at approximately 18:00, a third party called the kmcc emergency contact telephone number to report liquid leaking from the pig launcher door at the edna station. The kmcc controller initiated an emergency response line (erl) conference call with company subject matter experts to determine a course of action. A technician was dispatched to site and an update erl call was scheduled for when the technician arrived onsite. The technician arrived onsite and verified there was liquid leaking from the pig launcher door. The technician determined the leak was the result of a failed o-ring on the launcher door tattletale bolt. The update erl call was conducted at 19:17. The o-ring was replaired/replaced. Contaminated soil was cleaned up by early morning 3/29/14. Update 4/28/2014 supplemental/final report. No information updated within this report beyond this addition to teh narrative section. Dot data development team was trying to determine why we could not pick "o-ring" as a subcaluse under section g-6 of this report. The follow is their response: "the developer has informed me that your report does not need to have a sub-cause entered under part g6 due to it being a 'small spill'. I was also told that within the next month we will be releasing an update to odes 2.0 which will be removing the 'small spill' short form so that everyone will fill out the long form moving forward. Regards, data collection team"
Detailed record list
Report Received Date
2014-04-25 00:00:00
Iyear
2014
Report Number
20140166
Supplemental Number
19322
Report Type
Supplemental Final
Operator Id
32678
Name
Kinder Morgan Crude And Condensate Llc
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-03-28 18:00:00
Location Latitude
28.91382
Location Longitude
-96.628799
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4.5
Recovered Bbls
4.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-03-28 18:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
On Site Datetime
2014-03-28 19:20:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Kinder Morgan Crude Condensate - Edna Station
Segment Name
570kmcc-Ml 30" Edna To Missouri City
Onshore State Abbreviation
Tx
Onshore Postal Code
77957
Onshore City Name
Edna
Onshore County Name
Jackson
Designated Location
Milepost/valve Station
Designated Name
Plmp 54.94
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Scraper/pig Trap
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
428
Est Cost Prop Damage
100
Est Cost Emergency
0
Est Cost Environmental
45151
Est Cost Other
0
Prpty
45679
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
L**** K******
Preparer Title
Pipeline Engineer
Preparer Email
L************@k***********.com
Preparer Telephone
713-369-9707
Preparer Fax
713-336-4041
Prepared Date
2014-04-28 00:00:00
Authorizer Name
J**** H********
Authorizer Telephone
713-369-9443
Authorizer Title
Manager - Ccs
Authorizer Email
J**************@k***********.com
Narrative
On 3/28/14 at approximately 18:00, a third party called the kmcc emergency contact telephone number to report liquid leaking from the pig launcher door at the edna station. The kmcc controller initiated an emergency response line (erl) conference call with company subject matter experts to determine a course of action. A technician was dispatched to site and an update erl call was scheduled for when the technician arrived onsite. The technician arrived onsite and verified there was liquid leaking from the pig launcher door. The technician determined the leak was the result of a failed o-ring on the launcher door tattletale bolt. The update erl call was conducted at 19:17. The o-ring was replaired/replaced. Contaminated soil was cleaned up by early morning 3/29/14. Update 4/28/2014 supplemental/final report. No information updated within this report beyond this addition to teh narrative section. Dot data development team was trying to determine why we could not pick "o-ring" as a subcaluse under section g-6 of this report. The follow is their response: "the developer has informed me that your report does not need to have a sub-cause entered under part g6 due to it being a 'small spill'. I was also told that within the next month we will be releasing an update to odes 2.0 which will be removing the 'small spill' short form so that everyone will fill out the long form moving forward. Regards, data collection team"
| Report Received Date | 2014-04-25 00:00:00 |
|---|---|
| Iyear | 2014 |
| Report Number | 20140166 |
| Supplemental Number | 19322 |
| Report Type | Supplemental Final |
| Operator Id | 32678 PHMSA Enforcement |
| Name | Kinder Morgan Crude And Condensate Llc |
| Operator Street Address | 1001 Louisiana St., Suite 1000 |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2014-03-28 18:00:00 |
| Location Latitude | 28.91382 Google Maps OpenStreetMap |
| Location Longitude | -96.628799 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 4.5 |
| Recovered Bbls | 4.5 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2014-03-28 18:00:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| On Site Datetime | 2014-03-28 19:20:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Kinder Morgan Crude Condensate - Edna Station |
| Segment Name | 570kmcc-Ml 30" Edna To Missouri City |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77957 |
| Onshore City Name | Edna |
| Onshore County Name | Jackson |
| Designated Location | Milepost/valve Station |
| Designated Name | Plmp 54.94 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Scraper/pig Trap |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 428 |
| Est Cost Prop Damage | 100 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 45151 |
| Est Cost Other | 0 |
| Prpty | 45679 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Preparer Name | L**** K****** |
| Preparer Title | Pipeline Engineer |
| Preparer Email | L************@k***********.com |
| Preparer Telephone | 713-369-9707 |
| Preparer Fax | 713-336-4041 |
| Prepared Date | 2014-04-28 00:00:00 |
| Authorizer Name | J**** H******** |
| Authorizer Telephone | 713-369-9443 |
| Authorizer Title | Manager - Ccs |
| Authorizer Email | J**************@k***********.com |
| Narrative | On 3/28/14 at approximately 18:00, a third party called the kmcc emergency contact telephone number to report liquid leaking from the pig launcher door at the edna station. The kmcc controller initiated an emergency response line (erl) conference call with company subject matter experts to determine a course of action. A technician was dispatched to site and an update erl call was scheduled for when the technician arrived onsite. The technician arrived onsite and verified there was liquid leaking from the pig launcher door. The technician determined the leak was the result of a failed o-ring on the launcher door tattletale bolt. The update erl call was conducted at 19:17. The o-ring was replaired/replaced. Contaminated soil was cleaned up by early morning 3/29/14. Update 4/28/2014 supplemental/final report. No information updated within this report beyond this addition to teh narrative section. Dot data development team was trying to determine why we could not pick "o-ring" as a subcaluse under section g-6 of this report. The follow is their response: "the developer has informed me that your report does not need to have a sub-cause entered under part g6 due to it being a 'small spill'. I was also told that within the next month we will be releasing an update to odes 2.0 which will be removing the 'small spill' short form so that everyone will fill out the long form moving forward. Regards, data collection team" |
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