HL incident on 2014-03-31 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$205,120
Incident datetime
2014-03-31 13:00
Report number
Location
TX
Narrative
On 3/31/14 an enterprise technician was performing DOT valve inspections at mile post 45 when he discovered a gasoline / water mixture within a valve box located adjacent to the DOT block valve. Technicians cleaned up and removed the gasoline / water mixture and the contaminated soil from the valve box. The site was excavated to inspect the valve body. No active leak was observed at the time. Operations monitored the site, and no product leakage was observed. Upon visual inspection the next day a small packing leak was discovered. The pipeline was immediately shut down to repair the packing leak. The nrc was called due to the likelihood of costs exceeding $50,000. Nrc report # 107852 was generated. The valve was repaired and the pipeline was restarted 4/1/14 at 19:46. Operations remained on site to assure the valve was not leaking. No leaks were observed. The site was inspected again on 4/2/14 with no leakage; subsequently, the valve site was back-filled returning it to normal service. On 5/17/14 the line was shutdown to replace the valve. The valve was replaced and the line was restarted on 5/18/14.
Detailed record list
Report Received Date
2014-04-24 00:00:00
Iyear
2014
Report Number
20140161
Supplemental Number
19527
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-03-31 13:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.71
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-03-31 13:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-04-01 14:10:00
Restart Datetime
2014-04-01 19:46:00
On Site Datetime
2014-03-31 13:30:00
Nrc Rpt Datetime
2014-04-01 18:50:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Baytown To Beaumont # 1
Segment Name
P63
Onshore State Abbreviation
Tx
Onshore Postal Code
77705
Onshore City Name
Fannett
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Mp 45
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Inside Other Enclosed Space
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
1962
Manufactured Year
1959
Material Involved
Material Other Than Carbon Steel
Material Details
Valve Packing Material
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
205120
Est Cost Emergency
7405
Est Cost Environmental
182705
Est Cost Other
0
Prpty
395330
Accident Psig
120
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
142560
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Enterprise did not perform an investigation into the controller's actions as they were in no relation to the valve packing failure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Block Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Valve Packing Failure
Preparer Name
T* S*****
Preparer Title
Senior Pipeline Compliance Specialist
Preparer Email
T*******@e****.com
Preparer Telephone
713 381 6681
Preparer Fax
713 381 6811
Prepared Date
2014-07-01 00:00:00
Authorizer Name
T* S*****
Authorizer Telephone
713 381 6681
Authorizer Title
Senior Pipeline Compliance Specialist
Authorizer Email
T*******@e****.com
Narrative
On 3/31/14 an enterprise technician was performing DOT valve inspections at mile post 45 when he discovered a gasoline / water mixture within a valve box located adjacent to the DOT block valve. Technicians cleaned up and removed the gasoline / water mixture and the contaminated soil from the valve box. The site was excavated to inspect the valve body. No active leak was observed at the time. Operations monitored the site, and no product leakage was observed. Upon visual inspection the next day a small packing leak was discovered. The pipeline was immediately shut down to repair the packing leak. The nrc was called due to the likelihood of costs exceeding $50,000. Nrc report # 107852 was generated. The valve was repaired and the pipeline was restarted 4/1/14 at 19:46. Operations remained on site to assure the valve was not leaking. No leaks were observed. The site was inspected again on 4/2/14 with no leakage; subsequently, the valve site was back-filled returning it to normal service. On 5/17/14 the line was shutdown to replace the valve. The valve was replaced and the line was restarted on 5/18/14.
Report Received Date 2014-04-24 00:00:00
Iyear 2014
Report Number 20140161
Supplemental Number 19527
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-03-31 13:00:00
Location Latitude 29.935 Google Maps OpenStreetMap
Location Longitude -94.2833333 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.71
Recovered Bbls 0.71
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-03-31 13:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-04-01 14:10:00
Restart Datetime 2014-04-01 19:46:00
On Site Datetime 2014-03-31 13:30:00
Nrc Rpt Datetime 2014-04-01 18:50:00
Nrc Rpt Num 107852 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Baytown To Beaumont # 1
Segment Name P63
Onshore State Abbreviation Tx
Onshore Postal Code 77705
Onshore City Name Fannett
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name Mp 45
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Inside Other Enclosed Space
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Wkm
Installation Year 1962
Manufactured Year 1959
Material Involved Material Other Than Carbon Steel
Material Details Valve Packing Material
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 205120
Est Cost Emergency 7405
Est Cost Environmental 182705
Est Cost Other 0
Prpty 395330
Accident Psig 120
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 142560
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Enterprise did not perform an investigation into the controller's actions as they were in no relation to the valve packing failure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Block Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Valve Packing Failure
Preparer Name T* S*****
Preparer Title Senior Pipeline Compliance Specialist
Preparer Email T*******@e****.com
Preparer Telephone 713 381 6681
Preparer Fax 713 381 6811
Prepared Date 2014-07-01 00:00:00
Authorizer Name T* S*****
Authorizer Telephone 713 381 6681
Authorizer Title Senior Pipeline Compliance Specialist
Authorizer Email T*******@e****.com
Narrative On 3/31/14 an enterprise technician was performing DOT valve inspections at mile post 45 when he discovered a gasoline / water mixture within a valve box located adjacent to the DOT block valve. Technicians cleaned up and removed the gasoline / water mixture and the contaminated soil from the valve box. The site was excavated to inspect the valve body. No active leak was observed at the time. Operations monitored the site, and no product leakage was observed. Upon visual inspection the next day a small packing leak was discovered. The pipeline was immediately shut down to repair the packing leak. The nrc was called due to the likelihood of costs exceeding $50,000. Nrc report # 107852 was generated. The valve was repaired and the pipeline was restarted 4/1/14 at 19:46. Operations remained on site to assure the valve was not leaking. No leaks were observed. The site was inspected again on 4/2/14 with no leakage; subsequently, the valve site was back-filled returning it to normal service. On 5/17/14 the line was shutdown to replace the valve. The valve was replaced and the line was restarted on 5/18/14.

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