HL incident on 2014-03-27 — TX

Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-03-27 09:15
Report number
Location
TX
Narrative
On 3/27/2014 operations personnel discovered a crude oil release from a plug on the bonnet of the shell valve at tank 1404. Approximately one barrel was released. The affected soil was removed and remediated on site. The tank was out of service at the time of the release. An investigation revealed a loose plug on the bonnet of the shell valve which allowed crude oil to be released. The plug was removed, cleaned, re-taped and re-installed. The tank has subsequently been placed back in service on may 14, 2014.
Detailed record list
Report Received Date
2014-04-24 00:00:00
Iyear
2014
Report Number
20140160
Supplemental Number
19724
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-03-27 09:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2014-03-27 09:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Shut Down Not Required.tank Is Out Of Service.
On Site Datetime
2014-03-27 09:45:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Corsicana Station
Segment Name
Corsicana Station
Onshore State Abbreviation
Tx
Onshore Postal Code
75110
Onshore City Name
Corsicana
Onshore County Name
Navarro
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Plug On Tank Shell Valve.
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
2000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2000
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2014-09-15 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 3/27/2014 operations personnel discovered a crude oil release from a plug on the bonnet of the shell valve at tank 1404. Approximately one barrel was released. The affected soil was removed and remediated on site. The tank was out of service at the time of the release. An investigation revealed a loose plug on the bonnet of the shell valve which allowed crude oil to be released. The plug was removed, cleaned, re-taped and re-installed. The tank has subsequently been placed back in service on may 14, 2014.
Report Received Date 2014-04-24 00:00:00
Iyear 2014
Report Number 20140160
Supplemental Number 19724
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-03-27 09:15:00
Location Latitude 32.07175 Google Maps OpenStreetMap
Location Longitude -96.47357 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2014-03-27 09:15:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Shut Down Not Required.tank Is Out Of Service.
On Site Datetime 2014-03-27 09:45:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Corsicana Station
Segment Name Corsicana Station
Onshore State Abbreviation Tx
Onshore Postal Code 75110
Onshore City Name Corsicana
Onshore County Name Navarro
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Plug On Tank Shell Valve.
Release Type Leak
Leak Type Connection Failure
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 2000
Est Cost Environmental 0
Est Cost Other 0
Prpty 2000
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2014-09-15 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On 3/27/2014 operations personnel discovered a crude oil release from a plug on the bonnet of the shell valve at tank 1404. Approximately one barrel was released. The affected soil was removed and remediated on site. The tank was out of service at the time of the release. An investigation revealed a loose plug on the bonnet of the shell valve which allowed crude oil to be released. The plug was removed, cleaned, re-taped and re-installed. The tank has subsequently been placed back in service on may 14, 2014.

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