HL incident on 2014-03-25 — TX

Operator
Plantation Pipe Line Co
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-03-25 13:22
Report number
Location
TX
Narrative
While refilling the mdf scraper trap, the mechanical technician mistakenly opened a drain valve that he was intending to close. The failure to close this valve properly resulted in the west manifold separator to overflow, which released approximately 750 gallons of gasoline product.
Detailed record list
Report Received Date
2014-04-23 00:00:00
Iyear
2014
Report Number
20140158
Supplemental Number
19305
Report Type
Original Final
Operator Id
Name
Plantation Pipe Line Co
Operator Street Address
1001 Louisiana Street Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-03-25 13:22:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
17.85
Recovered Bbls
17.85
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2014-03-25 13:22:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Valve Mistakenly Opened To Cause The Release Was Immediately Closed
On Site Datetime
2014-03-25 13:22:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Collins Tank Farm
Onshore State Abbreviation
Ms
Onshore Postal Code
39428
Onshore City Name
Collins
Onshore County Name
Covington
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
140
Est Cost Prop Damage
0
Est Cost Emergency
18000
Est Cost Environmental
0
Est Cost Other
0
Prpty
18140
Accident Psig
0
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The control room had no involvement with this incident. The work being performed was conducted by local field operations.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
Q****** H* F******
Preparer Title
Manager-Compliance Codes And Standards
Preparer Email
Q**************@k***********.com
Preparer Telephone
770-751-4240
Preparer Fax
770-751-4130
Prepared Date
2014-04-23 00:00:00
Authorizer Name
Q****** H* F******
Authorizer Telephone
770-751-4240
Authorizer Title
Manager-Compliance Codes And Standards
Authorizer Email
Q**************@k***********.com
Narrative
While refilling the mdf scraper trap, the mechanical technician mistakenly opened a drain valve that he was intending to close. The failure to close this valve properly resulted in the west manifold separator to overflow, which released approximately 750 gallons of gasoline product.
Report Received Date 2014-04-23 00:00:00
Iyear 2014
Report Number 20140158
Supplemental Number 19305
Report Type Original Final
Operator Id 15674 PHMSA Enforcement
Name Plantation Pipe Line Co
Operator Street Address 1001 Louisiana Street Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-03-25 13:22:00
Location Latitude 31.636831 Google Maps OpenStreetMap
Location Longitude -89.523521 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 17.85
Recovered Bbls 17.85
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2014-03-25 13:22:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Valve Mistakenly Opened To Cause The Release Was Immediately Closed
On Site Datetime 2014-03-25 13:22:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Collins Tank Farm
Onshore State Abbreviation Ms
Onshore Postal Code 39428
Onshore City Name Collins
Onshore County Name Covington
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 140
Est Cost Prop Damage 0
Est Cost Emergency 18000
Est Cost Environmental 0
Est Cost Other 0
Prpty 18140
Accident Psig 0
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The control room had no involvement with this incident. The work being performed was conducted by local field operations.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name Q****** H* F******
Preparer Title Manager-Compliance Codes And Standards
Preparer Email Q**************@k***********.com
Preparer Telephone 770-751-4240
Preparer Fax 770-751-4130
Prepared Date 2014-04-23 00:00:00
Authorizer Name Q****** H* F******
Authorizer Telephone 770-751-4240
Authorizer Title Manager-Compliance Codes And Standards
Authorizer Email Q**************@k***********.com
Narrative While refilling the mdf scraper trap, the mechanical technician mistakenly opened a drain valve that he was intending to close. The failure to close this valve properly resulted in the west manifold separator to overflow, which released approximately 750 gallons of gasoline product.

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