HL incident on 2014-03-21 — TX

Operator
Plantation Pipe Line Co
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$55,000
Incident datetime
2014-03-21 17:20
Report number
Location
TX
Narrative
A property owner contacted the control center about an odor and dead vegetation. An investigation was initiated and a leaking pipeline was confirmed. Repair and cleanup operations were initiated. The cause for the failure is an original pipe manufacturing defect. The leak was due to a lamination in the seamless pipe that collected hydrogen and leaked due to due to a hydrogen blister and step-wise cracking.
Detailed record list
Report Received Date
2014-04-17 00:00:00
Iyear
2014
Report Number
20140155
Supplemental Number
33288
Report Type
Supplemental Final
Operator Id
Name
Plantation Pipe Line Co
Operator Street Address
1001 Louisiana Street Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-03-21 22:25:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
41
Recovered Bbls
16.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2014-03-21 17:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
This Pipeline Segment Was Already Shutdown When The Leak Was Discovered.
On Site Datetime
2014-03-21 17:35:00
Nrc Rpt Datetime
2014-03-21 23:09:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
14 Cnf
Segment Name
Line Section 6b
Onshore State Abbreviation
Ga
Onshore Postal Code
30180
Onshore City Name
Villa Rica
Onshore County Name
Carroll
Designated Location
Milepost/valve Station
Designated Name
444.4
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
14
Pipe Wall Thickness
0.375
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
S & L
Pipe Coating Type
Coal Tar
Installation Year
1951
Manufactured Year
1951
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Original Pipe Mfg Defect-Lamin
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
0
Rel Water Name
No Name For Groundwater
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
5000
Est Cost Prop Damage
55000
Est Cost Emergency
131500
Est Cost Environmental
329500
Est Cost Other
0
Prpty
521000
Accident Psig
1006
Mop Psig
1350
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
74612
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind
Yes
Invest No Schedule Ind Details
The Control Center Investigation At The Time Of The Incident Found That There Were No Indications A Controller Could Have Used To Recognize The Leak. It Was Also Determined That No Recent Controller Actions Had Resulted In Any Unfavorable Pressure Situations On This Segment Of The Pipeline.
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Original Pipe Manufacturing Defect-Lamination
Additional Lamination Ind
Yes
Collected Data Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Circ Wave Recent Year
2013
Geometry Recent Year
2013
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
Q****** H* F******
Preparer Title
Manager-Compliance Codes And Standards
Preparer Email
Q**************@k***********.com
Preparer Telephone
770-751-4240
Preparer Fax
770-751-4130
Prepared Date
2020-02-05 00:00:00
Authorizer Name
Q****** H* F******
Authorizer Telephone
770-751-4240
Authorizer Title
Manager-Compliance Codes And Standards
Authorizer Email
Q**************@k***********.com
Narrative
A property owner contacted the control center about an odor and dead vegetation. An investigation was initiated and a leaking pipeline was confirmed. Repair and cleanup operations were initiated. The cause for the failure is an original pipe manufacturing defect. The leak was due to a lamination in the seamless pipe that collected hydrogen and leaked due to due to a hydrogen blister and step-wise cracking.
Report Received Date 2014-04-17 00:00:00
Iyear 2014
Report Number 20140155
Supplemental Number 33288
Report Type Supplemental Final
Operator Id 15674 PHMSA Enforcement
Name Plantation Pipe Line Co
Operator Street Address 1001 Louisiana Street Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-03-21 22:25:00
Location Latitude 33.7161833 Google Maps OpenStreetMap
Location Longitude -84.9190558 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 41
Recovered Bbls 16.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2014-03-21 17:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain This Pipeline Segment Was Already Shutdown When The Leak Was Discovered.
On Site Datetime 2014-03-21 17:35:00
Nrc Rpt Datetime 2014-03-21 23:09:00
Nrc Rpt Num 1077368 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name 14 Cnf
Segment Name Line Section 6b
Onshore State Abbreviation Ga
Onshore Postal Code 30180
Onshore City Name Villa Rica
Onshore County Name Carroll
Designated Location Milepost/valve Station
Designated Name 444.4
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 14
Pipe Wall Thickness 0.375
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer S & L
Pipe Coating Type Coal Tar
Installation Year 1951
Manufactured Year 1951
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Original Pipe Mfg Defect-Lamin
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Groundwater Contam Ind Yes
Amount Released 0
Rel Water Name No Name For Groundwater
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 5000
Est Cost Prop Damage 55000
Est Cost Emergency 131500
Est Cost Environmental 329500
Est Cost Other 0
Prpty 521000
Accident Psig 1006
Mop Psig 1350
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 74612
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind Yes
Invest No Schedule Ind Details The Control Center Investigation At The Time Of The Incident Found That There Were No Indications A Controller Could Have Used To Recognize The Leak. It Was Also Determined That No Recent Controller Actions Had Resulted In Any Unfavorable Pressure Situations On This Segment Of The Pipeline.
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Original Pipe Manufacturing Defect-Lamination
Additional Lamination Ind Yes
Collected Data Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Circ Wave Recent Year 2013
Geometry Recent Year 2013
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name Q****** H* F******
Preparer Title Manager-Compliance Codes And Standards
Preparer Email Q**************@k***********.com
Preparer Telephone 770-751-4240
Preparer Fax 770-751-4130
Prepared Date 2020-02-05 00:00:00
Authorizer Name Q****** H* F******
Authorizer Telephone 770-751-4240
Authorizer Title Manager-Compliance Codes And Standards
Authorizer Email Q**************@k***********.com
Narrative A property owner contacted the control center about an odor and dead vegetation. An investigation was initiated and a leaking pipeline was confirmed. Repair and cleanup operations were initiated. The cause for the failure is an original pipe manufacturing defect. The leak was due to a lamination in the seamless pipe that collected hydrogen and leaked due to due to a hydrogen blister and step-wise cracking.

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