GTG incident on 2014-11-27 — KY

Operator
Southern Star Central Gas Pipeline, Inc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,100
Incident datetime
2014-11-27 03:20
Report number
Location
KY
Narrative
On 11/27/2014 at 03:20 ssc gas control began receiving alarms that lasted approximately 15 minutes. During this time the pressures on the "guymon 26in." were observed as decreasing and continued for approximately 40 minutes. Gas control attempted to investigate the potential cause and after no reasoning could be determined, ssc operations were called at 03:50. Ssc operations arrived at the wakita compressor station and confirmed with gas control, at 04:16, the cap on the relief valve was off and it was the expected cause of the drop in pressure. By 11:29 all relief valves between wakita station and the upstream alva station had been confirmed as not blowing. The set-points were tested on the relief and found to work correctly. The station piping was isolated until 12/2 when the relief was rebuilt and tested again.
Detailed record list
Report Received Date
2014-12-19 00:00:00
Iyear
2014
Report Number
20140145
Supplemental Number
16590
Report Type
Original Final
Operator Id
Name
Southern Star Central Gas Pipeline, Inc
Operator Street Address
4700 Highway 56; Box 20010
Operator City Name
Owensboro
Operator State Abbreviation
KY
Operator Postal Code
42301
Local Datetime
2014-11-27 03:17:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2014-11-27 05:55:00
Commodity Released Type
Natural Gas
Unintentional Release
3910
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
The Relief Valve Failed At The Wrong Set Point. The Relief Valve Was Shut In.
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2014-11-27 03:20:00
On Site Datetime
2014-11-27 04:16:00
On Off Shore
Onshore
Onshore State Abbreviation
Ok
Onshore Postal Code
73771
Onshore City Name
Wakita
Onshore County Name
Grant
Designated Location
Survey Station No.
Designated Name
150/10321+78
Pipe Fac Name
Wakita Station-Line N
Segment Name
Oklahoma Hugoton 26"
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Esd System, But Excluding Product Drain Lines And Tubing
Installation Year
1965
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
The Relief Valve Malfunctioned And Started To Relieve Gas Below The Set Point.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
236
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
16031
Est Cost Intentional Release
0
Est Cost Prop Damage
2100
Est Cost Emergency
1300
Est Cost Other
0
Prpty
19431
Accident Psig
542
Mop Psig
720
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Incorrect Action Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Additional Alarm Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Valve Began Blowing Below Set Point.
Preparer Name
D**** C*****
Preparer Title
Compliance Engineer
Preparer Email
D***********@s****.com
Preparer Telephone
2708524391
Authorizer Name
D**** S*******
Authorizer Title
Pipeline Compliance Manager
Authorizer Telephone
2708524424
Authorizer Email
D***************@s****.com
Narrative
On 11/27/2014 at 03:20 ssc gas control began receiving alarms that lasted approximately 15 minutes. During this time the pressures on the "guymon 26in." were observed as decreasing and continued for approximately 40 minutes. Gas control attempted to investigate the potential cause and after no reasoning could be determined, ssc operations were called at 03:50. Ssc operations arrived at the wakita compressor station and confirmed with gas control, at 04:16, the cap on the relief valve was off and it was the expected cause of the drop in pressure. By 11:29 all relief valves between wakita station and the upstream alva station had been confirmed as not blowing. The set-points were tested on the relief and found to work correctly. The station piping was isolated until 12/2 when the relief was rebuilt and tested again.
Report Received Date 2014-12-19 00:00:00
Iyear 2014
Report Number 20140145
Supplemental Number 16590
Report Type Original Final
Operator Id 31711 PHMSA Enforcement
Name Southern Star Central Gas Pipeline, Inc
Operator Street Address 4700 Highway 56; Box 20010
Operator City Name Owensboro
Operator State Abbreviation KY
Operator Postal Code 42301
Local Datetime 2014-11-27 03:17:00
Location Latitude 36.86646759 Google Maps OpenStreetMap
Location Longitude -97.9307755 Google Maps OpenStreetMap
Nrc Rpt Num 1102104 NRC Report How to search
Nrc Rpt Datetime 2014-11-27 05:55:00
Commodity Released Type Natural Gas
Unintentional Release 3910
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain The Relief Valve Failed At The Wrong Set Point. The Relief Valve Was Shut In.
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2014-11-27 03:20:00
On Site Datetime 2014-11-27 04:16:00
On Off Shore Onshore
Onshore State Abbreviation Ok
Onshore Postal Code 73771
Onshore City Name Wakita
Onshore County Name Grant
Designated Location Survey Station No.
Designated Name 150/10321+78
Pipe Fac Name Wakita Station-Line N
Segment Name Oklahoma Hugoton 26"
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Esd System, But Excluding Product Drain Lines And Tubing
Installation Year 1965
Material Involved Carbon Steel
Release Type Other
Release Type Details The Relief Valve Malfunctioned And Started To Relieve Gas Below The Set Point.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 236
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 16031
Est Cost Intentional Release 0
Est Cost Prop Damage 2100
Est Cost Emergency 1300
Est Cost Other 0
Prpty 19431
Accident Psig 542
Mop Psig 720
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Incorrect Action Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Additional Alarm Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Valve Began Blowing Below Set Point.
Preparer Name D**** C*****
Preparer Title Compliance Engineer
Preparer Email D***********@s****.com
Preparer Telephone 2708524391
Authorizer Name D**** S*******
Authorizer Title Pipeline Compliance Manager
Authorizer Telephone 2708524424
Authorizer Email D***************@s****.com
Narrative On 11/27/2014 at 03:20 ssc gas control began receiving alarms that lasted approximately 15 minutes. During this time the pressures on the "guymon 26in." were observed as decreasing and continued for approximately 40 minutes. Gas control attempted to investigate the potential cause and after no reasoning could be determined, ssc operations were called at 03:50. Ssc operations arrived at the wakita compressor station and confirmed with gas control, at 04:16, the cap on the relief valve was off and it was the expected cause of the drop in pressure. By 11:29 all relief valves between wakita station and the upstream alva station had been confirmed as not blowing. The set-points were tested on the relief and found to work correctly. The station piping was isolated until 12/2 when the relief was rebuilt and tested again.

All rights reserved. Copyright © by ClearPHMSA