GTG incident on 2014-11-28 — TX

Operator
Columbia Gulf Transmission, Llc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-11-28 03:22
Report number
Location
TX
Narrative
An 8-in blow-off valve failed to close after inadvertently releasing for the second time material into atmosphere. The emergency shutdown was not activated. It was identified that this valve failed to close due to a solenoid valve had a spring that was improperly seated. A root cause analysis investigation identified that the valve failed to close thus allowing the material to flow through the valve until it was controlled by compressor station personnel. A change to the programmable logic control settings was completed, tested the system and then returned into service. The facility was monitored to ensure that the same error will not be regenerated. No further issues were noted.
Detailed record list
Report Received Date
2014-12-17 00:00:00
Iyear
2014
Report Number
20140141
Supplemental Number
17247
Report Type
Supplemental Final
Operator Id
Name
Columbia Gulf Transmission, Llc
Operator Street Address
700 Louisiana St. Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-11-28 03:22:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2014-11-28 05:39:00
Commodity Released Type
Natural Gas
Unintentional Release
16431
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
The Facility Was Restarted After Idenitifying And Correcting The Plc Error.
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2014-11-28 03:22:00
On Site Datetime
2014-11-28 03:49:00
On Off Shore
Onshore
Onshore State Abbreviation
Ky
Onshore Postal Code
42539
Onshore City Name
Liberty
Onshore County Name
Casey County
Designated Location
Milepost
Designated Name
Shafer Act
Pipe Fac Name
Clementsville Compressor Station
Segment Name
2sh-1dbd
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2013
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Programmable Logic Controller Setting
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
238
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
60138
Est Cost Intentional Release
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Other
0
Est Cost Other Details
No Other Costs Were Noted
Prpty
60138
Accident Psig
660
Mop Psig
935
Mop Cfr Section
192.619(A)(2)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller did perform as he was trained and qualified to do so and responded accordingly. He had no interaction with any valve commands before the alarms were noted.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Compressor Or Compressor-Related Equipment
Eq Failure Type
Compressor Or Compressor-Related Equipment
Other Compressor Ind
Other
Other Compressor Details
8-In Blow-Off Valve
Eq Additional Other Ind
Yes
Eq Additional Other Details
Internal Spring Was Out Of Position
Preparer Name
G***** H*****
Preparer Title
Engineer
Preparer Email
G************@t**********.com
Preparer Telephone
(304) 357-3728
Authorizer Name
L** R*****
Authorizer Title
Manger Us Regulatory Compliance
Authorizer Telephone
(832)320-5315
Authorizer Email
L*********@t**********.com
Narrative
An 8-in blow-off valve failed to close after inadvertently releasing for the second time material into atmosphere. The emergency shutdown was not activated. It was identified that this valve failed to close due to a solenoid valve had a spring that was improperly seated. A root cause analysis investigation identified that the valve failed to close thus allowing the material to flow through the valve until it was controlled by compressor station personnel. A change to the programmable logic control settings was completed, tested the system and then returned into service. The facility was monitored to ensure that the same error will not be regenerated. No further issues were noted.
Report Received Date 2014-12-17 00:00:00
Iyear 2014
Report Number 20140141
Supplemental Number 17247
Report Type Supplemental Final
Operator Id 2620 PHMSA Enforcement
Name Columbia Gulf Transmission, Llc
Operator Street Address 700 Louisiana St. Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-11-28 03:22:00
Location Latitude 37.31 Google Maps OpenStreetMap
Location Longitude -85.061136 Google Maps OpenStreetMap
Nrc Rpt Num 1102136 NRC Report How to search
Nrc Rpt Datetime 2014-11-28 05:39:00
Commodity Released Type Natural Gas
Unintentional Release 16431
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain The Facility Was Restarted After Idenitifying And Correcting The Plc Error.
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2014-11-28 03:22:00
On Site Datetime 2014-11-28 03:49:00
On Off Shore Onshore
Onshore State Abbreviation Ky
Onshore Postal Code 42539
Onshore City Name Liberty
Onshore County Name Casey County
Designated Location Milepost
Designated Name Shafer Act
Pipe Fac Name Clementsville Compressor Station
Segment Name 2sh-1dbd
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2013
Material Involved Carbon Steel
Release Type Other
Release Type Details Programmable Logic Controller Setting
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 238
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 60138
Est Cost Intentional Release 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Other 0
Est Cost Other Details No Other Costs Were Noted
Prpty 60138
Accident Psig 660
Mop Psig 935
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller did perform as he was trained and qualified to do so and responded accordingly. He had no interaction with any valve commands before the alarms were noted.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Compressor Or Compressor-Related Equipment
Eq Failure Type Compressor Or Compressor-Related Equipment
Other Compressor Ind Other
Other Compressor Details 8-In Blow-Off Valve
Eq Additional Other Ind Yes
Eq Additional Other Details Internal Spring Was Out Of Position
Preparer Name G***** H*****
Preparer Title Engineer
Preparer Email G************@t**********.com
Preparer Telephone (304) 357-3728
Authorizer Name L** R*****
Authorizer Title Manger Us Regulatory Compliance
Authorizer Telephone (832)320-5315
Authorizer Email L*********@t**********.com
Narrative An 8-in blow-off valve failed to close after inadvertently releasing for the second time material into atmosphere. The emergency shutdown was not activated. It was identified that this valve failed to close due to a solenoid valve had a spring that was improperly seated. A root cause analysis investigation identified that the valve failed to close thus allowing the material to flow through the valve until it was controlled by compressor station personnel. A change to the programmable logic control settings was completed, tested the system and then returned into service. The facility was monitored to ensure that the same error will not be regenerated. No further issues were noted.

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