GTG incident on 2014-12-03 — OK

Operator
Williams Energy, Llc
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,733,406
Incident datetime
2014-12-03 15:00
Report number
Location
OK
Narrative
A dive company was setting mats to cover and protect a newly installed valve assembly on the discovery 18 inch pipeline at a depth of 230 feet. An unexpected current caused the mat to catch on the 2 inch by-pass line which damaged the piping and caused the release. The line was quickly isolated and repaired. The diver was not injured and there was no other damage as a result of this incident. There was no sheen reported on the water. Additional nrc notification was made by williams at the same time witt o'brien's was making notification. Williams number is 1102550.
Detailed record list
Report Received Date
2014-12-15 00:00:00
Iyear
2014
Report Number
20140136
Supplemental Number
16771
Report Type
Supplemental Final
Operator Id
Name
Williams Energy, Llc
Operator Street Address
One Williams Center P.o. Box 645
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2014-12-03 15:00:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2014-12-03 15:14:00
Commodity Released Type
Natural Gas
Unintentional Release
11000
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
Able To Isolate The Bypass
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2014-12-03 15:00:00
On Site Datetime
2014-12-03 15:00:00
On Off Shore
Offshore
Off Water Depth
220
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
South Timbalier
Off Ocs Block
231
Off Area Accident Type
Below Water, Pipe On Or Above Seabed
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Drain Lines
Installation Year
1997
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Broken Piping On Bypass Valve
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
660
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
42500
Est Cost Intentional Release
0
Est Cost Prop Damage
2733406
Est Cost Emergency
0
Est Cost Other
0
Prpty
2775906
Accident Psig
700
Mop Psig
1850
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Sub-Sea Connection
Pipeline Function
Offshore Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Contractor broke valve assembly while setting mats.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name
S**** F******
Preparer Title
Pipeline Safety Engineer
Preparer Email
S************@w*******.com
Preparer Telephone
713-215-3051
Authorizer Name
S**** F******
Authorizer Title
Pipeline Safety Engineer
Authorizer Telephone
713-215-3051
Authorizer Email
S************@w*******.com
Narrative
A dive company was setting mats to cover and protect a newly installed valve assembly on the discovery 18 inch pipeline at a depth of 230 feet. An unexpected current caused the mat to catch on the 2 inch by-pass line which damaged the piping and caused the release. The line was quickly isolated and repaired. The diver was not injured and there was no other damage as a result of this incident. There was no sheen reported on the water. Additional nrc notification was made by williams at the same time witt o'brien's was making notification. Williams number is 1102550.
Report Received Date 2014-12-15 00:00:00
Iyear 2014
Report Number 20140136
Supplemental Number 16771
Report Type Supplemental Final
Operator Id 30940 PHMSA Enforcement
Name Williams Energy, Llc
Operator Street Address One Williams Center P.o. Box 645
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2014-12-03 15:00:00
Location Latitude 28.3614 Google Maps OpenStreetMap
Location Longitude -90.1975 Google Maps OpenStreetMap
Nrc Rpt Num 1102545 NRC Report How to search
Nrc Rpt Datetime 2014-12-03 15:14:00
Commodity Released Type Natural Gas
Unintentional Release 11000
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain Able To Isolate The Bypass
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2014-12-03 15:00:00
On Site Datetime 2014-12-03 15:00:00
On Off Shore Offshore
Off Water Depth 220
Off Accident Origin On The Outer Continental Shelf (Ocs)
Off Ocs Area South Timbalier
Off Ocs Block 231
Off Area Accident Type Below Water, Pipe On Or Above Seabed
Pipe Facility Type Interstate
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
Item Involved Drain Lines
Installation Year 1997
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Broken Piping On Bypass Valve
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 660
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 42500
Est Cost Intentional Release 0
Est Cost Prop Damage 2733406
Est Cost Emergency 0
Est Cost Other 0
Prpty 2775906
Accident Psig 700
Mop Psig 1850
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Internal Inspection Ind Yes
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Sub-Sea Connection
Pipeline Function Offshore Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Contractor broke valve assembly while setting mats.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name S**** F******
Preparer Title Pipeline Safety Engineer
Preparer Email S************@w*******.com
Preparer Telephone 713-215-3051
Authorizer Name S**** F******
Authorizer Title Pipeline Safety Engineer
Authorizer Telephone 713-215-3051
Authorizer Email S************@w*******.com
Narrative A dive company was setting mats to cover and protect a newly installed valve assembly on the discovery 18 inch pipeline at a depth of 230 feet. An unexpected current caused the mat to catch on the 2 inch by-pass line which damaged the piping and caused the release. The line was quickly isolated and repaired. The diver was not injured and there was no other damage as a result of this incident. There was no sheen reported on the water. Additional nrc notification was made by williams at the same time witt o'brien's was making notification. Williams number is 1102550.

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