GTG incident on 2014-09-02 — TX

Operator
Columbia Gas Transmission, Llc
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2014-09-02 22:10
Report number
Location
TX
Narrative
On tuesday, september 2, 2014, millennium pipeline company, llc's hancock compressor station (cs) located in delaware county, ny was in the path of a line of severe thunderstorms traveling through the region. Hancock cs is covered under columbia gas transmission, llc operator id 2616. A lightning strike damaged an electric transformer that feeds hancock cs area, causing loss of commercial electrical power. During the power outage, the station's emergency generator started but power failed to fully transfer to the station's reserve power in an amount of time causing station's pneumatic compressors to fault (and not restart). The loss of pneumatic pressure caused the station emergency shutdown vent valves to open. However, due to the station's low pneumatic pressure switch failing to trigger a station emergency shutdown, the station isolation (block) valves remained in the open position causing the unintended release of natural gas into atmosphere. Working with the generator vendor, adjustments were made to the generator's response settings and the station's low pneumatic pressure switch to prevent a similar fault from future re-occurrence. The days following this incident, several tests were conducted to each system, then the entire facility to ensure the successful start of the back-up generator in the event of a commercial electric power loss as well as the correct operation of the low pneumatic pressure switch, as it was designed to operate. During the testing, the back-up generator started successfully whenever the commercial electric power was disconnected from the main bus power system and the low-pressure switch functioned with no failures being noted. There were no similar events or interruptions to the facility's back-up electric power generator of the facility when commercial electric power was interrupted.
Detailed record list
Report Received Date
2014-10-01 00:00:00
Iyear
2014
Report Number
20140101
Supplemental Number
35547
Report Type
Supplemental Final
Operator Id
Name
Columbia Gas Transmission, Llc
Operator Street Address
700 Louisiana St. Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-09-02 22:10:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2014-09-03 02:02:00
Commodity Released Type
Natural Gas
Unintentional Release
9060
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
The Transmission Pipeline Continued The Flow In Bypass Mode
Communication State Fed Ind
No
Ignite Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2014-09-02 22:10:00
On Site Datetime
2014-09-02 23:25:00
On Off Shore
Onshore
Onshore State Abbreviation
Ny
Onshore Postal Code
12760
Onshore City Name
Long Eddy
Onshore County Name
Delaware County
Designated Location
Not Applicable
Pipe Fac Name
Hancock Compressor Station
Segment Name
Hancock
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2014
Manufactured Year
2014
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Esd Valve Failed To Close
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
215
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
35696
Est Cost Intentional Release
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
3.94
Prpty
35696
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
905
Gas Flow In Pipe In Mcf
876.5
Mop Psig
1350
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2014-03-14 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Not Mandated
Gas Required Odorized Ind
Yes
Gas Odorized Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No investigation of the controller or the control room since this incident was initiated by an external factor (loss of commercial electric power feed to the facility).
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Other Natural Force Damage
Natural Force Type
Other Natural Force Damage
Nf Other Details
A Line Of Severe Thunderstorms Was Traversing The Area That Generated A Line Of Lightning Strikes Interrupting Commercial Power To The Facility.
Nf Extreme Weather Ind
Yes
Nf Other Ind
Yes
Nf Extreme Weather Details
Severe Thunderstorms Associated With Lightning Strikes.
Nf Lightning Ind
Yes
Preparer Name
W****** Y****
Preparer Title
Us Regulatory Compliance Specialist
Preparer Email
W************@t*******.com
Preparer Telephone
304-410-2818
Authorizer Name
P*** S******
Authorizer Title
Manager Us Regulatory Compliance East
Authorizer Telephone
304-550-4866
Authorizer Email
P***********@t*******.com
Narrative
On tuesday, september 2, 2014, millennium pipeline company, llc's hancock compressor station (cs) located in delaware county, ny was in the path of a line of severe thunderstorms traveling through the region. Hancock cs is covered under columbia gas transmission, llc operator id 2616. A lightning strike damaged an electric transformer that feeds hancock cs area, causing loss of commercial electrical power. During the power outage, the station's emergency generator started but power failed to fully transfer to the station's reserve power in an amount of time causing station's pneumatic compressors to fault (and not restart). The loss of pneumatic pressure caused the station emergency shutdown vent valves to open. However, due to the station's low pneumatic pressure switch failing to trigger a station emergency shutdown, the station isolation (block) valves remained in the open position causing the unintended release of natural gas into atmosphere. Working with the generator vendor, adjustments were made to the generator's response settings and the station's low pneumatic pressure switch to prevent a similar fault from future re-occurrence. The days following this incident, several tests were conducted to each system, then the entire facility to ensure the successful start of the back-up generator in the event of a commercial electric power loss as well as the correct operation of the low pneumatic pressure switch, as it was designed to operate. During the testing, the back-up generator started successfully whenever the commercial electric power was disconnected from the main bus power system and the low-pressure switch functioned with no failures being noted. There were no similar events or interruptions to the facility's back-up electric power generator of the facility when commercial electric power was interrupted.
Report Received Date 2014-10-01 00:00:00
Iyear 2014
Report Number 20140101
Supplemental Number 35547
Report Type Supplemental Final
Operator Id 2616 PHMSA Enforcement
Name Columbia Gas Transmission, Llc
Operator Street Address 700 Louisiana St. Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-09-02 22:10:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 41.88366 Google Maps OpenStreetMap
Location Longitude -75.14228 Google Maps OpenStreetMap
Nrc Rpt Num 1094204 NRC Report How to search
Nrc Rpt Datetime 2014-09-03 02:02:00
Commodity Released Type Natural Gas
Unintentional Release 9060
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain The Transmission Pipeline Continued The Flow In Bypass Mode
Communication State Fed Ind No
Ignite Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2014-09-02 22:10:00
On Site Datetime 2014-09-02 23:25:00
On Off Shore Onshore
Onshore State Abbreviation Ny
Onshore Postal Code 12760
Onshore City Name Long Eddy
Onshore County Name Delaware County
Designated Location Not Applicable
Pipe Fac Name Hancock Compressor Station
Segment Name Hancock
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2014
Manufactured Year 2014
Material Involved Carbon Steel
Release Type Other
Release Type Details Esd Valve Failed To Close
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 215
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 35696
Est Cost Intentional Release 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 3.94
Prpty 35696
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 905
Gas Flow In Pipe In Mcf 876.5
Mop Psig 1350
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2014-03-14 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Not Mandated
Gas Required Odorized Ind Yes
Gas Odorized Ind Yes
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No investigation of the controller or the control room since this incident was initiated by an external factor (loss of commercial electric power feed to the facility).
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Other Natural Force Damage
Natural Force Type Other Natural Force Damage
Nf Other Details A Line Of Severe Thunderstorms Was Traversing The Area That Generated A Line Of Lightning Strikes Interrupting Commercial Power To The Facility.
Nf Extreme Weather Ind Yes
Nf Other Ind Yes
Nf Extreme Weather Details Severe Thunderstorms Associated With Lightning Strikes.
Nf Lightning Ind Yes
Preparer Name W****** Y****
Preparer Title Us Regulatory Compliance Specialist
Preparer Email W************@t*******.com
Preparer Telephone 304-410-2818
Authorizer Name P*** S******
Authorizer Title Manager Us Regulatory Compliance East
Authorizer Telephone 304-550-4866
Authorizer Email P***********@t*******.com
Narrative On tuesday, september 2, 2014, millennium pipeline company, llc's hancock compressor station (cs) located in delaware county, ny was in the path of a line of severe thunderstorms traveling through the region. Hancock cs is covered under columbia gas transmission, llc operator id 2616. A lightning strike damaged an electric transformer that feeds hancock cs area, causing loss of commercial electrical power. During the power outage, the station's emergency generator started but power failed to fully transfer to the station's reserve power in an amount of time causing station's pneumatic compressors to fault (and not restart). The loss of pneumatic pressure caused the station emergency shutdown vent valves to open. However, due to the station's low pneumatic pressure switch failing to trigger a station emergency shutdown, the station isolation (block) valves remained in the open position causing the unintended release of natural gas into atmosphere. Working with the generator vendor, adjustments were made to the generator's response settings and the station's low pneumatic pressure switch to prevent a similar fault from future re-occurrence. The days following this incident, several tests were conducted to each system, then the entire facility to ensure the successful start of the back-up generator in the event of a commercial electric power loss as well as the correct operation of the low pneumatic pressure switch, as it was designed to operate. During the testing, the back-up generator started successfully whenever the commercial electric power was disconnected from the main bus power system and the low-pressure switch functioned with no failures being noted. There were no similar events or interruptions to the facility's back-up electric power generator of the facility when commercial electric power was interrupted.

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