GTG incident on 2014-07-26 — TX

Operator
Anr Pipeline Co
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$235,000
Incident datetime
2014-07-26 17:38
Report number
Location
TX
Narrative
On 26 july 2014, a third-party helicopter patrol observed a release of gas located in west cameron block 165 (29.37260800, -93.54129500) south of cameron parish in the gulf of mexico. The leak was reported to anr pipeline company, operator for tc offshore, as an approximately ten foot in diameter bubbling over the location of tc offshore's 687 transmission pipeline. The section of 687 line containing the leak was shut in by a check valve on the downstream side and by closing a valve on the upstream side. No sheen or product was reported at the surface of the water. Following the section being shut in, contract employees were deployed to the site to investigate and repair the leak. Prior to the arrival of the contractors, helicopter patrols were conducted in the area to monitor the leak and conditions of the site. No sheen or product was reported for the duration of aerial monitoring while the pipeline was being repaired. On 29 july, anr and contract personnel from cal-dive international arrived at the leak location in west cameron block 165 to inspect the pipe and repair the leak. At approximately 12:00 cdt, divers entered the water and determined the location of the leak. After determining the approximate location of the leak, pipeline pressure was reduced to 80 psig water, and water blasting was used to remove the concrete coating from the pipe to prepare for the installation of a plidco ten inch bolt-on clamp over the leak. The clamp was then installed according to manufacturer specifications, the exposed pipe wrapped in syntho-glass, and pipeline backfilled. Finally, the pipeline was monitored during repressurization to confirm that the leak was sucessfully repaired.
Detailed record list
Report Received Date
2014-08-25 00:00:00
Iyear
2014
Report Number
20140091
Supplemental Number
16480
Report Type
Original Final
Operator Id
Name
Anr Pipeline Co
Operator Street Address
700 Louisiana Street Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2014-07-26 17:38:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2014-07-26 18:20:00
Commodity Released Type
Natural Gas
Unintentional Release
1
Intentional Release
2261
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-07-26 17:38:00
Restart Datetime
2014-07-31 06:55:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2014-07-26 17:38:00
On Site Datetime
2014-07-29 08:10:00
On Off Shore
Offshore
Off Water Depth
49
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
West Cameron
Off Ocs Block
165
Off Area Accident Type
Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10.75
Pipe Wall Thickness
0.365
Pipe Smys
42000
Pipe Specification
Api-5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Epoxy
Installation Year
2006
Manufactured Year
2005
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
327
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
4
Est Cost Intentional Release
8730
Est Cost Prop Damage
235000
Est Cost Emergency
0
Est Cost Other
0
Prpty
243734
Accident Psig
775
Mop Psig
1300
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Automatic
Length Segment Isolated
45725
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Lateral Line Hot Taps Into Another Lateral
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Hot Taps Into Another Line
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The small size of the defect and the amount of gas leaking
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R**** R* S*****
Preparer Title
Field Compliance Specialist
Preparer Email
R***********@t**********.com
Preparer Telephone
8325702966
Authorizer Name
R**** S*****
Authorizer Title
Field Compliance Specialist
Authorizer Telephone
832-570-2966
Authorizer Email
R***********@t**********.com
Narrative
On 26 july 2014, a third-party helicopter patrol observed a release of gas located in west cameron block 165 (29.37260800, -93.54129500) south of cameron parish in the gulf of mexico. The leak was reported to anr pipeline company, operator for tc offshore, as an approximately ten foot in diameter bubbling over the location of tc offshore's 687 transmission pipeline. The section of 687 line containing the leak was shut in by a check valve on the downstream side and by closing a valve on the upstream side. No sheen or product was reported at the surface of the water. Following the section being shut in, contract employees were deployed to the site to investigate and repair the leak. Prior to the arrival of the contractors, helicopter patrols were conducted in the area to monitor the leak and conditions of the site. No sheen or product was reported for the duration of aerial monitoring while the pipeline was being repaired. On 29 july, anr and contract personnel from cal-dive international arrived at the leak location in west cameron block 165 to inspect the pipe and repair the leak. At approximately 12:00 cdt, divers entered the water and determined the location of the leak. After determining the approximate location of the leak, pipeline pressure was reduced to 80 psig water, and water blasting was used to remove the concrete coating from the pipe to prepare for the installation of a plidco ten inch bolt-on clamp over the leak. The clamp was then installed according to manufacturer specifications, the exposed pipe wrapped in syntho-glass, and pipeline backfilled. Finally, the pipeline was monitored during repressurization to confirm that the leak was sucessfully repaired.
Report Received Date 2014-08-25 00:00:00
Iyear 2014
Report Number 20140091
Supplemental Number 16480
Report Type Original Final
Operator Id 405 PHMSA Enforcement
Name Anr Pipeline Co
Operator Street Address 700 Louisiana Street Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2014-07-26 17:38:00
Location Latitude 29.372608 Google Maps OpenStreetMap
Location Longitude -93.541295 Google Maps OpenStreetMap
Nrc Rpt Num 1090355 NRC Report How to search
Nrc Rpt Datetime 2014-07-26 18:20:00
Commodity Released Type Natural Gas
Unintentional Release 1
Intentional Release 2261
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-07-26 17:38:00
Restart Datetime 2014-07-31 06:55:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2014-07-26 17:38:00
On Site Datetime 2014-07-29 08:10:00
On Off Shore Offshore
Off Water Depth 49
Off Accident Origin On The Outer Continental Shelf (Ocs)
Off Ocs Area West Cameron
Off Ocs Block 165
Off Area Accident Type Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type Interstate
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10.75
Pipe Wall Thickness 0.365
Pipe Smys 42000
Pipe Specification Api-5l
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Epoxy
Installation Year 2006
Manufactured Year 2005
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 327
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 4
Est Cost Intentional Release 8730
Est Cost Prop Damage 235000
Est Cost Emergency 0
Est Cost Other 0
Prpty 243734
Accident Psig 775
Mop Psig 1300
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Automatic
Length Segment Isolated 45725
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Lateral Line Hot Taps Into Another Lateral
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Hot Taps Into Another Line
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The small size of the defect and the amount of gas leaking
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R**** R* S*****
Preparer Title Field Compliance Specialist
Preparer Email R***********@t**********.com
Preparer Telephone 8325702966
Authorizer Name R**** S*****
Authorizer Title Field Compliance Specialist
Authorizer Telephone 832-570-2966
Authorizer Email R***********@t**********.com
Narrative On 26 july 2014, a third-party helicopter patrol observed a release of gas located in west cameron block 165 (29.37260800, -93.54129500) south of cameron parish in the gulf of mexico. The leak was reported to anr pipeline company, operator for tc offshore, as an approximately ten foot in diameter bubbling over the location of tc offshore's 687 transmission pipeline. The section of 687 line containing the leak was shut in by a check valve on the downstream side and by closing a valve on the upstream side. No sheen or product was reported at the surface of the water. Following the section being shut in, contract employees were deployed to the site to investigate and repair the leak. Prior to the arrival of the contractors, helicopter patrols were conducted in the area to monitor the leak and conditions of the site. No sheen or product was reported for the duration of aerial monitoring while the pipeline was being repaired. On 29 july, anr and contract personnel from cal-dive international arrived at the leak location in west cameron block 165 to inspect the pipe and repair the leak. At approximately 12:00 cdt, divers entered the water and determined the location of the leak. After determining the approximate location of the leak, pipeline pressure was reduced to 80 psig water, and water blasting was used to remove the concrete coating from the pipe to prepare for the installation of a plidco ten inch bolt-on clamp over the leak. The clamp was then installed according to manufacturer specifications, the exposed pipe wrapped in syntho-glass, and pipeline backfilled. Finally, the pipeline was monitored during repressurization to confirm that the leak was sucessfully repaired.

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