GD incident on 2014-08-10 — NY

Operator
Niagara Mohawk Power Corp
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2014-08-10 15:00
Report number
Location
NY, Not Within a County or Parish
Narrative
An explosion occurred at 310 paige street prompting the shutdown of the gas service line to this dwelling. The root cause of the incident indicates that the cause of the incident was gas escaping from a fractured gas line inside the premises, beyond the meter of this property later found to be vacant. The leak was the result of trespassers cutting and removing segments of gas piping inside the premises prior to the explosion.. The service was permanently retired on august 10, 2014.National grid billing records indicate that the electric and gas services to both units were inactive from march 2013 through the date of the incident. The gas service was discontinued by the company via 'soft closure,' where no mechanical device or fitting was installed at the service valve to prevent the flow of gas. The company used 'soft closure' because the service valves and meters were inside the residence, and the company claims it could not gain access to physically lock them. A contributing factor to this incident was national grid's policy in place at the time and decision not to physically lock the gas service line valves and/or physically disconnect the customer piping from the gas supply, when the service was discontinued.
Detailed record list
Occurred At
2014-08-10 15:00:00
Year
2014
Report Received Date
2014-09-10 00:00:00
Iyear
2014.0
Report Number
20140078.0
Supplemental Number
16224.0
Report Type
Supplemental Final
Operator Id
Name
Niagara Mohawk Power Corp
Operator Street Address
300 Erie Boulevard West
Operator City Name
Syracuse
Operator State Abbreviation
NY
Operator Postal Code
13202
Local Datetime
2014-08-10 15:00:00
Location Street Address
310 Paige St.
Location City Name
Schenectady
Location County Name
Not Within A County Or Parish
Location State Abbreviation
NY
Location Postal Code
12307
Location Latitude
Location Longitude
Nrc Rpt Datetime
2014-08-10 16:38:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
5.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
Yes
Num Pub Evacuated
0.0
Incident Identified Datetime
2014-08-10 15:00:00
On Site Datetime
2014-08-10 16:00:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Service
Installation Year
1937.0
Pipe Diameter
1.25
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Other
Release Type Details
The Post-Incident Investigation Indicates That The Cause Of The Incident Was Gas Escaping From A Fractured Gas Line Inside The Premises, Beyond The Meter. The Leak Was The Result Of Trespassers Cutting And Removing Segments Of Customer Gas Piping Inside The Premises Prior To The Explosion.
Class Location Type
Class 4 Location
Est Cost Oper Paid
120000.0
Est Cost Prop Damage
5000.0
Est Cost Emergency
15000.0
Est Cost Other
0.0
Est Cost Unintentional Release
0.0
Prpty
140000.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
8.3
Normal Psig
8.0
Mop Psig
12.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Other
Accident Details
Gas Dispatch Called Gso
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
View only of scada no control
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Incident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
The Post-Incident Investigation Indicates That The Cause Of The Incident Was Gas Escaping From A Fractured Gas Line Inside The Premises, Beyond The Meter Of This Property Later Determined To Be Vacant. The Leak Was The Result Of Trespassers Cutting And Removing Segments Of Gas Piping Inside The Premises Prior To The Explosion.
Preparer Name
B**** J* D******
Preparer Title
Lead Supervisor Upstate Dispatch And Scheduling
Preparer Email
B************@n***********.com
Preparer Telephone
315-460-2035
Preparer Fax
315-460-2762
Authorizer Name
B**** P********
Authorizer Title
Manager Upstate Dispatch And Scheduling
Authorizer Telephone
315-460-2635
Authorizer Email
B**************@n***********.com
Narrative
An explosion occurred at 310 paige street prompting the shutdown of the gas service line to this dwelling. The root cause of the incident indicates that the cause of the incident was gas escaping from a fractured gas line inside the premises, beyond the meter of this property later found to be vacant. The leak was the result of trespassers cutting and removing segments of gas piping inside the premises prior to the explosion.. The service was permanently retired on august 10, 2014.National grid billing records indicate that the electric and gas services to both units were inactive from march 2013 through the date of the incident. The gas service was discontinued by the company via 'soft closure,' where no mechanical device or fitting was installed at the service valve to prevent the flow of gas. The company used 'soft closure' because the service valves and meters were inside the residence, and the company claims it could not gain access to physically lock them. A contributing factor to this incident was national grid's policy in place at the time and decision not to physically lock the gas service line valves and/or physically disconnect the customer piping from the gas supply, when the service was discontinued.
Occurred At 2014-08-10 15:00:00
Year 2014
Report Received Date 2014-09-10 00:00:00
Iyear 2014.0
Report Number 20140078.0
Supplemental Number 16224.0
Report Type Supplemental Final
Operator Id 13480 PHMSA Enforcement
Name Niagara Mohawk Power Corp
Operator Street Address 300 Erie Boulevard West
Operator City Name Syracuse
Operator State Abbreviation NY
Operator Postal Code 13202
Local Datetime 2014-08-10 15:00:00
Location Street Address 310 Paige St.
Location City Name Schenectady
Location County Name Not Within A County Or Parish
Location State Abbreviation NY
Location Postal Code 12307
Location Latitude 42.8079 Google Maps OpenStreetMap
Location Longitude -73.93872 Google Maps OpenStreetMap
Nrc Rpt Datetime 2014-08-10 16:38:00
Nrc Rpt Num 1091862 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 5.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind Yes
Num Pub Evacuated 0.0
Incident Identified Datetime 2014-08-10 15:00:00
On Site Datetime 2014-08-10 16:00:00
Federal No
Location Type Private Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Service
Installation Year 1937.0
Pipe Diameter 1.25
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Other
Release Type Details The Post-Incident Investigation Indicates That The Cause Of The Incident Was Gas Escaping From A Fractured Gas Line Inside The Premises, Beyond The Meter. The Leak Was The Result Of Trespassers Cutting And Removing Segments Of Customer Gas Piping Inside The Premises Prior To The Explosion.
Class Location Type Class 4 Location
Est Cost Oper Paid 120000.0
Est Cost Prop Damage 5000.0
Est Cost Emergency 15000.0
Est Cost Other 0.0
Est Cost Unintentional Release 0.0
Prpty 140000.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 8.3
Normal Psig 8.0
Mop Psig 12.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Other
Accident Details Gas Dispatch Called Gso
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details View only of scada no control
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Incident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details The Post-Incident Investigation Indicates That The Cause Of The Incident Was Gas Escaping From A Fractured Gas Line Inside The Premises, Beyond The Meter Of This Property Later Determined To Be Vacant. The Leak Was The Result Of Trespassers Cutting And Removing Segments Of Gas Piping Inside The Premises Prior To The Explosion.
Preparer Name B**** J* D******
Preparer Title Lead Supervisor Upstate Dispatch And Scheduling
Preparer Email B************@n***********.com
Preparer Telephone 315-460-2035
Preparer Fax 315-460-2762
Authorizer Name B**** P********
Authorizer Title Manager Upstate Dispatch And Scheduling
Authorizer Telephone 315-460-2635
Authorizer Email B**************@n***********.com
Narrative An explosion occurred at 310 paige street prompting the shutdown of the gas service line to this dwelling. The root cause of the incident indicates that the cause of the incident was gas escaping from a fractured gas line inside the premises, beyond the meter of this property later found to be vacant. The leak was the result of trespassers cutting and removing segments of gas piping inside the premises prior to the explosion.. The service was permanently retired on august 10, 2014.National grid billing records indicate that the electric and gas services to both units were inactive from march 2013 through the date of the incident. The gas service was discontinued by the company via 'soft closure,' where no mechanical device or fitting was installed at the service valve to prevent the flow of gas. The company used 'soft closure' because the service valves and meters were inside the residence, and the company claims it could not gain access to physically lock them. A contributing factor to this incident was national grid's policy in place at the time and decision not to physically lock the gas service line valves and/or physically disconnect the customer piping from the gas supply, when the service was discontinued.

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