HL incident on 2014-01-17 — TX

Operator
Bkep Pipeline, Llc
Cause
Other Accident Cause
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,050
Incident datetime
2014-01-17 10:48
Report number
Location
TX
Narrative
James potter was operating in the control center at 10:48 am when the discharge pressure at depew dropped from 362psi to 285psi. The flow rate on the west trunk flow meter at cushing also dropped from 395bph to 321bph. James shut down the west trunk pipeline at 10:53am to relieve pressure on the line. Leslie armstrong was routed to depew to check and isolate the station. Windall mayes was routed down the pipeline right of way looking for leaks. Windall mayes located the leak at 12:12pm. The leak was caused by a shot from a firearm that pierced the pipeline.
Detailed record list
Report Received Date
2014-02-17 00:00:00
Iyear
2014
Report Number
20140057
Supplemental Number
19476
Report Type
Supplemental Final
Operator Id
Name
Bkep Pipeline, Llc
Operator Street Address
2277 Plaza Drive Suite 500
Operator City Name
Sugar Land
Operator State Abbreviation
TX
Operator Postal Code
77479
Local Datetime
2014-01-17 10:48:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
25
Recovered Bbls
25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2014-01-17 10:48:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2014-01-17 10:53:00
Restart Datetime
2014-01-18 08:20:00
On Site Datetime
2014-01-17 12:12:00
Nrc Rpt Datetime
2014-01-17 16:59:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
West Trunk Pipeline
Onshore State Abbreviation
Ok
Onshore Postal Code
74028
Onshore City Name
Rural
Onshore County Name
Creek
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
In Or Spanning An Open Ditch
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6.62
Pipe Wall Thickness
0.28
Pipe Smys
35000
Pipe Specification
Grade B
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1932
Manufactured Year
1932
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
The Pipeline Was Shot With A Firearm Twice With One Shot Penetrating The Pipe Wall.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
5000
Est Cost Gas Released
0
Est Cost Prop Damage
2050
Est Cost Emergency
17000
Est Cost Environmental
6500
Est Cost Other
0
Prpty
30550
Accident Psig
362
Mop Psig
425
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
115100
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident occured due to intentional damage by unknown individual
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
Intentional Damage To Pipeline. Pipeline Was Shot Multiple Times By An Unknown Party And One Shot Penetrated The Pipe Wall.
Preparer Name
G*** M*****
Preparer Title
Manager Of Dot Pipeline Compliance
Preparer Email
G******@b***.com
Preparer Telephone
405-278-6405
Preparer Fax
405-278-6403
Prepared Date
2014-06-17 00:00:00
Authorizer Name
G*** M*****
Authorizer Telephone
405-278-6405
Authorizer Title
Manager Of Dot Pipeline Compliance
Authorizer Email
G******@b***.com
Narrative
James potter was operating in the control center at 10:48 am when the discharge pressure at depew dropped from 362psi to 285psi. The flow rate on the west trunk flow meter at cushing also dropped from 395bph to 321bph. James shut down the west trunk pipeline at 10:53am to relieve pressure on the line. Leslie armstrong was routed to depew to check and isolate the station. Windall mayes was routed down the pipeline right of way looking for leaks. Windall mayes located the leak at 12:12pm. The leak was caused by a shot from a firearm that pierced the pipeline.
Report Received Date 2014-02-17 00:00:00
Iyear 2014
Report Number 20140057
Supplemental Number 19476
Report Type Supplemental Final
Operator Id 32551 PHMSA Enforcement
Name Bkep Pipeline, Llc
Operator Street Address 2277 Plaza Drive Suite 500
Operator City Name Sugar Land
Operator State Abbreviation TX
Operator Postal Code 77479
Local Datetime 2014-01-17 10:48:00
Location Latitude 35.8377778 Google Maps OpenStreetMap
Location Longitude -96.5122222 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 25
Recovered Bbls 25
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2014-01-17 10:48:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2014-01-17 10:53:00
Restart Datetime 2014-01-18 08:20:00
On Site Datetime 2014-01-17 12:12:00
Nrc Rpt Datetime 2014-01-17 16:59:00
Nrc Rpt Num 1071462 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name West Trunk Pipeline
Onshore State Abbreviation Ok
Onshore Postal Code 74028
Onshore City Name Rural
Onshore County Name Creek
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype In Or Spanning An Open Ditch
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6.62
Pipe Wall Thickness 0.28
Pipe Smys 35000
Pipe Specification Grade B
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1932
Manufactured Year 1932
Material Involved Carbon Steel
Release Type Other
Release Type Details The Pipeline Was Shot With A Firearm Twice With One Shot Penetrating The Pipe Wall.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 5000
Est Cost Gas Released 0
Est Cost Prop Damage 2050
Est Cost Emergency 17000
Est Cost Environmental 6500
Est Cost Other 0
Prpty 30550
Accident Psig 362
Mop Psig 425
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 115100
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident occured due to intentional damage by unknown individual
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details Intentional Damage To Pipeline. Pipeline Was Shot Multiple Times By An Unknown Party And One Shot Penetrated The Pipe Wall.
Preparer Name G*** M*****
Preparer Title Manager Of Dot Pipeline Compliance
Preparer Email G******@b***.com
Preparer Telephone 405-278-6405
Preparer Fax 405-278-6403
Prepared Date 2014-06-17 00:00:00
Authorizer Name G*** M*****
Authorizer Telephone 405-278-6405
Authorizer Title Manager Of Dot Pipeline Compliance
Authorizer Email G******@b***.com
Narrative James potter was operating in the control center at 10:48 am when the discharge pressure at depew dropped from 362psi to 285psi. The flow rate on the west trunk flow meter at cushing also dropped from 395bph to 321bph. James shut down the west trunk pipeline at 10:53am to relieve pressure on the line. Leslie armstrong was routed to depew to check and isolate the station. Windall mayes was routed down the pipeline right of way looking for leaks. Windall mayes located the leak at 12:12pm. The leak was caused by a shot from a firearm that pierced the pipeline.

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