HL incident on 2013-12-05 — OH

Operator
Marathon Pipe Line Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$173,000
Incident datetime
2013-12-05 17:30
Report number
Location
OH
Narrative
Discovery made when an employee witnessed a small flange leak. - all systems and the station were shutdown. -verified integrity of all associated flanges and equipment including relpacement of multiple gaskets. - approximately, 8.5 cubic yards of contaminated soil was removed from the site.
Detailed record list
Report Received Date
2013-12-30 00:00:00
Iyear
2013
Report Number
20130411
Supplemental Number
20041
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2013-12-05 17:30:00
Location Latitude
Location Longitude
-89.06510432
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-12-05 17:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Already Down, Per Schedule
On Site Datetime
2013-12-05 17:30:00
Nrc Rpt Datetime
2013-12-05 18:13:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Capline Station (Patoka)
Segment Name
Crossover Line
Onshore State Abbreviation
Il
Onshore Postal Code
62892
Onshore City Name
Vernon
Onshore County Name
Marion
Designated Location
Milepost/valve Station
Designated Name
1754+31
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1968
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
173000
Est Cost Emergency
122000
Est Cost Environmental
0
Est Cost Other
0
Prpty
295030
Accident Psig
438
Mop Psig
275
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Related No Proc Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
R**** H********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
4194212121
Prepared Date
2015-01-09 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
4194212121
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
Discovery made when an employee witnessed a small flange leak. - all systems and the station were shutdown. -verified integrity of all associated flanges and equipment including relpacement of multiple gaskets. - approximately, 8.5 cubic yards of contaminated soil was removed from the site.
Report Received Date 2013-12-30 00:00:00
Iyear 2013
Report Number 20130411
Supplemental Number 20041
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2013-12-05 17:30:00
Location Latitude 38.7893921 Google Maps OpenStreetMap
Location Longitude -89.06510432 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2013-12-05 17:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Already Down, Per Schedule
On Site Datetime 2013-12-05 17:30:00
Nrc Rpt Datetime 2013-12-05 18:13:00
Nrc Rpt Num 1067694 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Capline Station (Patoka)
Segment Name Crossover Line
Onshore State Abbreviation Il
Onshore Postal Code 62892
Onshore City Name Vernon
Onshore County Name Marion
Designated Location Milepost/valve Station
Designated Name 1754+31
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1968
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 173000
Est Cost Emergency 122000
Est Cost Environmental 0
Est Cost Other 0
Prpty 295030
Accident Psig 438
Mop Psig 275
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Pipeline Or Equipment Overpressured
Operation Type Pipeline Or Equipment Overpressured
Related No Proc Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name R**** H********
Preparer Title Hes Professional
Preparer Email R**********@m****************.com
Preparer Telephone 4194212121
Prepared Date 2015-01-09 00:00:00
Authorizer Name R****** B*****
Authorizer Telephone 4194212121
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative Discovery made when an employee witnessed a small flange leak. - all systems and the station were shutdown. -verified integrity of all associated flanges and equipment including relpacement of multiple gaskets. - approximately, 8.5 cubic yards of contaminated soil was removed from the site.

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