HL incident on 2013-11-20 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2013-11-20 15:20
Report number
Location
TX
Narrative
While onsite an enterprise technician observed an incorrect valve sequence shutdown. Third party control room gave a closed command to all their tank valves which also closed the sump valve. To prevent this from reoccurring the logic has been removed from the plc to disable the closure of the sump valve. Area was promptly cleaned up and returned to service.
Detailed record list
Report Received Date
2013-12-19 00:00:00
Iyear
2013
Report Number
20130402
Supplemental Number
20549
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-11-20 15:20:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-11-20 15:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-11-20 15:20:00
Restart Datetime
2013-11-20 16:30:00
On Site Datetime
2013-11-20 15:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Jal Meter Station
Segment Name
Jal Meter Station
Onshore State Abbreviation
Nm
Onshore Postal Code
88252
Onshore City Name
Jal
Onshore County Name
Lea
Designated Location
Survey Station No.
Designated Name
Jal
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
25
Est Cost Prop Damage
1000
Est Cost Emergency
0
Est Cost Environmental
6000
Est Cost Other
0
Prpty
7025
Accident Psig
5
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room and controller were not a contributing factor.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Other
Overflow Other Details
Incorrect Logic In Plc
Related Other Ind
Yes
Operation Related Details
Incorrect Logic In Plc
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
C**** A******
Preparer Title
Pipeline Compliance Specialist
Preparer Email
C*******@e****.com
Preparer Telephone
713-381-6426
Prepared Date
2015-06-25 00:00:00
Authorizer Name
C**** A******
Authorizer Telephone
713-381-6426
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
C*******@e****.com
Narrative
While onsite an enterprise technician observed an incorrect valve sequence shutdown. Third party control room gave a closed command to all their tank valves which also closed the sump valve. To prevent this from reoccurring the logic has been removed from the plc to disable the closure of the sump valve. Area was promptly cleaned up and returned to service.
Report Received Date 2013-12-19 00:00:00
Iyear 2013
Report Number 20130402
Supplemental Number 20549
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-11-20 15:20:00
Location Latitude 32.079424 Google Maps OpenStreetMap
Location Longitude -103.178079 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.2
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2013-11-20 15:20:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-11-20 15:20:00
Restart Datetime 2013-11-20 16:30:00
On Site Datetime 2013-11-20 15:20:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Jal Meter Station
Segment Name Jal Meter Station
Onshore State Abbreviation Nm
Onshore Postal Code 88252
Onshore City Name Jal
Onshore County Name Lea
Designated Location Survey Station No.
Designated Name Jal
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Meter/prover
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 25
Est Cost Prop Damage 1000
Est Cost Emergency 0
Est Cost Environmental 6000
Est Cost Other 0
Prpty 7025
Accident Psig 5
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room and controller were not a contributing factor.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Other
Overflow Other Details Incorrect Logic In Plc
Related Other Ind Yes
Operation Related Details Incorrect Logic In Plc
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name C**** A******
Preparer Title Pipeline Compliance Specialist
Preparer Email C*******@e****.com
Preparer Telephone 713-381-6426
Prepared Date 2015-06-25 00:00:00
Authorizer Name C**** A******
Authorizer Telephone 713-381-6426
Authorizer Title Pipeline Compliance Specialist
Authorizer Email C*******@e****.com
Narrative While onsite an enterprise technician observed an incorrect valve sequence shutdown. Third party control room gave a closed command to all their tank valves which also closed the sump valve. To prevent this from reoccurring the logic has been removed from the plc to disable the closure of the sump valve. Area was promptly cleaned up and returned to service.

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