HL incident on 2013-11-23 — OH

Operator
Marathon Pipe Line Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$874,500
Incident datetime
2013-11-23 11:00
Report number
Location
OH
Narrative
During a station inspection, an employee spotted crude oil on the ground - the pipeline station was shutdown as a precaution and station isolation was confirmed. - mpl response team was put in place and determined the source of the leak. The pipe was replaced. -30 cubic yards of contaminated soil was removed. Note: the pipeline was shutdown prior to the accident (11/22/2013 @ 15:15) but the system does not allow a date and time to be entered prior to the accident date and time.
Detailed record list
Report Received Date
2013-12-17 00:00:00
Iyear
2013
Report Number
20130399
Supplemental Number
19489
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2013-11-23 11:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
20
Recovered Bbls
20
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-11-23 11:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-11-23 11:00:00
Restart Datetime
2013-11-23 14:47:00
On Site Datetime
2013-11-23 11:30:00
Nrc Rpt Datetime
2013-11-23 12:05:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lebanon Station
Onshore State Abbreviation
In
Onshore Postal Code
46052
Onshore City Name
Lebanon
Onshore County Name
Boone
Designated Location
Milepost/valve Station
Designated Name
94.9
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Installation Year
1970
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1485
Est Cost Prop Damage
874500
Est Cost Emergency
144000
Est Cost Environmental
0
Est Cost Other
0
Prpty
1019985
Accident Psig
5
Mop Psig
257
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
R**** S********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2014-06-19 00:00:00
Authorizer Name
R****** W* B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory And Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
D**********************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ ******************************************************************************************************.
Report Received Date 2013-12-17 00:00:00
Iyear 2013
Report Number 20130399
Supplemental Number 19489
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2013-11-23 11:00:00
Location Latitude 40.039849 Google Maps OpenStreetMap
Location Longitude -86.409788 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 20
Recovered Bbls 20
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2013-11-23 11:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-11-23 11:00:00
Restart Datetime 2013-11-23 14:47:00
On Site Datetime 2013-11-23 11:30:00
Nrc Rpt Datetime 2013-11-23 12:05:00
Nrc Rpt Num 1066669 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lebanon Station
Onshore State Abbreviation In
Onshore Postal Code 46052
Onshore City Name Lebanon
Onshore County Name Boone
Designated Location Milepost/valve Station
Designated Name 94.9
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Interstate
Item Involved Relief Line And Relief Equipment
Installation Year 1970
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1485
Est Cost Prop Damage 874500
Est Cost Emergency 144000
Est Cost Environmental 0
Est Cost Other 0
Prpty 1019985
Accident Psig 5
Mop Psig 257
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name R**** S********
Preparer Title Hes Professional
Preparer Email R**********@m****************.com
Preparer Telephone 419-421-2121
Prepared Date 2014-06-19 00:00:00
Authorizer Name R****** W* B*****
Authorizer Telephone 419-421-2121
Authorizer Title Regulatory And Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative D**********************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************************@ ******************************************************************************************************.

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