HL incident on 2013-11-14 — TX

Operator
Enbridge Energy Marketing Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$23,000
Incident datetime
2013-11-14 07:12
Report number
Location
TX
Narrative
On november 14, 2013 at 0712 cst a crude oil leak, of approximately one barrel, occured on the tinsley 8" pipeline near rolling fork, sharkey county, ms. Enbridge houston control center received a call at 0712 cst on 11/14/13 from a landowner about a possible leak on his property from the tinsley 8" pipeline. The control center notified local operations of the possible leak at 0714 cst. At 0716 cst operation immediately shut down the pumps at the tinsley station and began emergency operations to isolate the section. Operations arrived at the possible leak site at 0756 cst and made confirmation the leak was from the tinsley 8" pipeline. At 0810 equipment arrived on-site, allowing operation to construct an earthen dam to contain the crude oil leak. The national response center was telephonically notified of the incident on 11/14/13 at 0913 cst. Evcavation revealed a pinhole leak which appears to be caused by internal corrosion. A temporary clamp was installed on the pipeline while clean-up and soil remediation occured. The msdeq and the US epa both made on-site visits and approved of the clean-up and remediation. A new section of pipe was installed on 11/16/13 and the pipeline was restarted on 11/17/13. The failed section of pipe was sent to a laboratory for failure analysis. Enbridge is still awaiting results of the failure analysis and will submit a supplemental report once additional data is analyzed and cause can be determined. Supplemental report submitted on 2/3/14 to correctly identify the type of interanl corrosion, in part g, identified by the third party lab analysis. Please find attached, a copy of the lab analysis performed by stress engineering services on the failed section of pipe for additional details and conclusions.
Detailed record list
Report Received Date
2013-12-16 00:00:00
Iyear
2013
Report Number
20130397
Supplemental Number
18974
Report Type
Supplemental Final
Operator Id
Name
Enbridge Energy Marketing Llc
Operator Street Address
1100 Louisiana, Suite 3300
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-11-14 07:12:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2013-11-14 07:12:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-11-14 07:16:00
Restart Datetime
2013-11-17 07:30:00
On Site Datetime
2013-11-14 07:56:00
Nrc Rpt Datetime
2013-11-14 09:13:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Tinsley 8"
Onshore State Abbreviation
Ms
Onshore Postal Code
39159
Onshore City Name
Rolling Fork
Onshore County Name
Sharkey
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.214
Pipe Smys
24000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
None
Manufactured Year
1940
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
23000
Est Cost Emergency
11000
Est Cost Environmental
25000
Est Cost Other
5000
Est Cost Other Details
Excavation, Pipe Replacement, Er Equipment, Supplies, Labor And Soil Remediation
Prpty
64100
Accident Psig
51
Mop Psig
600
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
Yes
Ultrasonic Ind
Yes
Ultrasonic Recent Year
2012
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2012
Hydrtst Most Rcnt Pressure
898
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
A***** G*****
Preparer Title
Compliance Coordinator
Preparer Email
A************@e*******.com
Preparer Telephone
713-353-5650
Prepared Date
2014-02-03 00:00:00
Authorizer Name
A***** G*****
Authorizer Telephone
713-353-5650
Authorizer Title
Compliance Coordinator
Authorizer Email
A************@e*******.com
Narrative
On november 14, 2013 at 0712 cst a crude oil leak, of approximately one barrel, occured on the tinsley 8" pipeline near rolling fork, sharkey county, ms. Enbridge houston control center received a call at 0712 cst on 11/14/13 from a landowner about a possible leak on his property from the tinsley 8" pipeline. The control center notified local operations of the possible leak at 0714 cst. At 0716 cst operation immediately shut down the pumps at the tinsley station and began emergency operations to isolate the section. Operations arrived at the possible leak site at 0756 cst and made confirmation the leak was from the tinsley 8" pipeline. At 0810 equipment arrived on-site, allowing operation to construct an earthen dam to contain the crude oil leak. The national response center was telephonically notified of the incident on 11/14/13 at 0913 cst. Evcavation revealed a pinhole leak which appears to be caused by internal corrosion. A temporary clamp was installed on the pipeline while clean-up and soil remediation occured. The msdeq and the US epa both made on-site visits and approved of the clean-up and remediation. A new section of pipe was installed on 11/16/13 and the pipeline was restarted on 11/17/13. The failed section of pipe was sent to a laboratory for failure analysis. Enbridge is still awaiting results of the failure analysis and will submit a supplemental report once additional data is analyzed and cause can be determined. Supplemental report submitted on 2/3/14 to correctly identify the type of interanl corrosion, in part g, identified by the third party lab analysis. Please find attached, a copy of the lab analysis performed by stress engineering services on the failed section of pipe for additional details and conclusions.
Report Received Date 2013-12-16 00:00:00
Iyear 2013
Report Number 20130397
Supplemental Number 18974
Report Type Supplemental Final
Operator Id 31423 PHMSA Enforcement
Name Enbridge Energy Marketing Llc
Operator Street Address 1100 Louisiana, Suite 3300
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-11-14 07:12:00
Location Latitude 32.842833 Google Maps OpenStreetMap
Location Longitude -90.905417 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2013-11-14 07:12:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-11-14 07:16:00
Restart Datetime 2013-11-17 07:30:00
On Site Datetime 2013-11-14 07:56:00
Nrc Rpt Datetime 2013-11-14 09:13:00
Nrc Rpt Num 1065712 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Tinsley 8"
Onshore State Abbreviation Ms
Onshore Postal Code 39159
Onshore City Name Rolling Fork
Onshore County Name Sharkey
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.214
Pipe Smys 24000
Pipe Specification Api 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type None
Manufactured Year 1940
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 23000
Est Cost Emergency 11000
Est Cost Environmental 25000
Est Cost Other 5000
Est Cost Other Details Excavation, Pipe Replacement, Er Equipment, Supplies, Labor And Soil Remediation
Prpty 64100
Accident Psig 51
Mop Psig 600
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind Yes
Ultrasonic Ind Yes
Ultrasonic Recent Year 2012
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2012
Hydrtst Most Rcnt Pressure 898
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name A***** G*****
Preparer Title Compliance Coordinator
Preparer Email A************@e*******.com
Preparer Telephone 713-353-5650
Prepared Date 2014-02-03 00:00:00
Authorizer Name A***** G*****
Authorizer Telephone 713-353-5650
Authorizer Title Compliance Coordinator
Authorizer Email A************@e*******.com
Narrative On november 14, 2013 at 0712 cst a crude oil leak, of approximately one barrel, occured on the tinsley 8" pipeline near rolling fork, sharkey county, ms. Enbridge houston control center received a call at 0712 cst on 11/14/13 from a landowner about a possible leak on his property from the tinsley 8" pipeline. The control center notified local operations of the possible leak at 0714 cst. At 0716 cst operation immediately shut down the pumps at the tinsley station and began emergency operations to isolate the section. Operations arrived at the possible leak site at 0756 cst and made confirmation the leak was from the tinsley 8" pipeline. At 0810 equipment arrived on-site, allowing operation to construct an earthen dam to contain the crude oil leak. The national response center was telephonically notified of the incident on 11/14/13 at 0913 cst. Evcavation revealed a pinhole leak which appears to be caused by internal corrosion. A temporary clamp was installed on the pipeline while clean-up and soil remediation occured. The msdeq and the US epa both made on-site visits and approved of the clean-up and remediation. A new section of pipe was installed on 11/16/13 and the pipeline was restarted on 11/17/13. The failed section of pipe was sent to a laboratory for failure analysis. Enbridge is still awaiting results of the failure analysis and will submit a supplemental report once additional data is analyzed and cause can be determined. Supplemental report submitted on 2/3/14 to correctly identify the type of interanl corrosion, in part g, identified by the third party lab analysis. Please find attached, a copy of the lab analysis performed by stress engineering services on the failed section of pipe for additional details and conclusions.

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