HL incident on 2013-11-27 — FL

Operator
Thunder Basin Pipeline, Llc
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2013-11-27 10:30
Report number
Location
FL
Narrative
Pipeline manager was flying with our patrol pilot on 11/27/2013. As they passed over the lebar junction, they noticed oil spraying out of a valve inside the facility. Manager called an employee to notify the control center to have the line shut down and for him (the employee) to proceed to the facility and isolate the leaking valve. The pipeline pumping station pump and motor were locked out and tagged out to prevent further operation of oil movements in the pipeline. Contractors were called to help in the clean up. Oily dirt was hauled to tds landfarm in torrington, wy and fresh dirt was hauled in to replace the contaminated soil. The valve that failed was replaced. Clean-up was completed on 12/02/2013. The pipeline was placed back in service on 11/30/2013 with a spotter at the leak site to verify that the pipeline was no longer leaking.
Detailed record list
Report Received Date
2013-12-06 00:00:00
Iyear
2013
Report Number
20130390
Supplemental Number
18800
Report Type
Original Final
Operator Id
Name
Thunder Basin Pipeline, Llc
Operator Street Address
5568 Woodbine Road Suite 82
Operator City Name
Pace
Operator State Abbreviation
FL
Operator Postal Code
32571
Local Datetime
2013-11-27 10:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-11-27 10:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-11-27 10:30:00
Restart Datetime
2013-11-30 19:41:00
On Site Datetime
2013-11-27 10:50:00
Nrc Rpt Datetime
2013-11-27 17:34:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Pipe Fac Name
Lebar Junction
Segment Name
Southwell Draw To Keenan
Onshore State Abbreviation
Wy
Onshore Postal Code
82633
Onshore City Name
Douglas
Onshore County Name
Converse
Designated Location
Milepost/valve Station
Designated Name
2.65
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2013
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
5000
Est Cost Gas Released
1200
Est Cost Prop Damage
2000
Est Cost Emergency
3000
Est Cost Environmental
75000
Est Cost Other
0
Prpty
86200
Accident Psig
600
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
20
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Temperature
Natural Force Type
Temperature
Temperature Subtype
Frozen Components
Nf Extreme Weather Ind
No
Preparer Name
J***** L* S******
Preparer Title
Wyoming Asset Manager
Preparer Email
J************@g****.com
Preparer Telephone
713-823-0331
Prepared Date
2013-12-06 00:00:00
Authorizer Name
J*** R* J*****
Authorizer Telephone
713-860-2605
Authorizer Title
Manager Of Dot Compliance And Facility Security
Authorizer Email
J**********@g****.com
Narrative
Pipeline manager was flying with our patrol pilot on 11/27/2013. As they passed over the lebar junction, they noticed oil spraying out of a valve inside the facility. Manager called an employee to notify the control center to have the line shut down and for him (the employee) to proceed to the facility and isolate the leaking valve. The pipeline pumping station pump and motor were locked out and tagged out to prevent further operation of oil movements in the pipeline. Contractors were called to help in the clean up. Oily dirt was hauled to tds landfarm in torrington, wy and fresh dirt was hauled in to replace the contaminated soil. The valve that failed was replaced. Clean-up was completed on 12/02/2013. The pipeline was placed back in service on 11/30/2013 with a spotter at the leak site to verify that the pipeline was no longer leaking.
Report Received Date 2013-12-06 00:00:00
Iyear 2013
Report Number 20130390
Supplemental Number 18800
Report Type Original Final
Operator Id 38894 PHMSA Enforcement
Name Thunder Basin Pipeline, Llc
Operator Street Address 5568 Woodbine Road Suite 82
Operator City Name Pace
Operator State Abbreviation FL
Operator Postal Code 32571
Local Datetime 2013-11-27 10:30:00
Location Latitude 42.917984 Google Maps OpenStreetMap
Location Longitude -105.240693 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2013-11-27 10:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-11-27 10:30:00
Restart Datetime 2013-11-30 19:41:00
On Site Datetime 2013-11-27 10:50:00
Nrc Rpt Datetime 2013-11-27 17:34:00
Nrc Rpt Num 1067028 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Pipe Fac Name Lebar Junction
Segment Name Southwell Draw To Keenan
Onshore State Abbreviation Wy
Onshore Postal Code 82633
Onshore City Name Douglas
Onshore County Name Converse
Designated Location Milepost/valve Station
Designated Name 2.65
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2013
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Gasket Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 5000
Est Cost Gas Released 1200
Est Cost Prop Damage 2000
Est Cost Emergency 3000
Est Cost Environmental 75000
Est Cost Other 0
Prpty 86200
Accident Psig 600
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 20
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Temperature
Natural Force Type Temperature
Temperature Subtype Frozen Components
Nf Extreme Weather Ind No
Preparer Name J***** L* S******
Preparer Title Wyoming Asset Manager
Preparer Email J************@g****.com
Preparer Telephone 713-823-0331
Prepared Date 2013-12-06 00:00:00
Authorizer Name J*** R* J*****
Authorizer Telephone 713-860-2605
Authorizer Title Manager Of Dot Compliance And Facility Security
Authorizer Email J**********@g****.com
Narrative Pipeline manager was flying with our patrol pilot on 11/27/2013. As they passed over the lebar junction, they noticed oil spraying out of a valve inside the facility. Manager called an employee to notify the control center to have the line shut down and for him (the employee) to proceed to the facility and isolate the leaking valve. The pipeline pumping station pump and motor were locked out and tagged out to prevent further operation of oil movements in the pipeline. Contractors were called to help in the clean up. Oily dirt was hauled to tds landfarm in torrington, wy and fresh dirt was hauled in to replace the contaminated soil. The valve that failed was replaced. Clean-up was completed on 12/02/2013. The pipeline was placed back in service on 11/30/2013 with a spotter at the leak site to verify that the pipeline was no longer leaking.

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