HL incident on 2013-11-03 — TX

Operator
Mobil Corp
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$58,000
Incident datetime
2013-11-03 18:00
Report number
Location
TX
Narrative
When the release was discovered it did not appear that notification to the nrc would be required, however due to the location and logistics of transporting personnel and equipment to the site it was determined that the $50,000 criteria would be met. An nrc report was made at that time. Propane was bubbling through standing water in a low area, no sheen, emulsion or other visible water impact was observed during the release. [requested update 3/24/2020: release investigation determined it was seam weep from a penetrator-type lack of fusion at the seam (seam crack). This feature was repaired on november 7, 2013 by installation of a plidco clamp and recoating the pipe with type 2 wax tape.]
Detailed record list
Report Received Date
2013-12-03 00:00:00
Iyear
2013
Report Number
20130386
Supplemental Number
33537
Report Type
Supplemental Final
Operator Id
Name
Mobil Corp
Operator Street Address
22777 Springwoods Village Parkway
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2013-11-03 13:50:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
1.2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2013-11-03 18:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-11-03 20:38:00
Restart Datetime
2013-11-08 08:00:00
On Site Datetime
2013-11-03 18:00:00
Nrc Rpt Datetime
2013-11-04 09:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Mr-114 Propane
Segment Name
Hull To Beaumont
Onshore State Abbreviation
Tx
Onshore Postal Code
77564
Onshore City Name
Hull
Onshore County Name
Hardin
Designated Location
Survey Station No.
Designated Name
95+25
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
16
Pipe Wall Thickness
0.25
Pipe Smys
46000
Pipe Specification
X-46
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Republic
Pipe Coating Type
Coal Tar
Installation Year
1958
Manufactured Year
1958
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
58000
Est Cost Emergency
30000
Est Cost Environmental
0
Est Cost Other
0
Prpty
88100
Accident Psig
498
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
87900
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a small leak, there were no alarms or controlroom information that indicated a leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Seam Crack
Additional Crack Ind
Yes
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Emat Ind
Yes
Axial Recent Year
2009
Circ Wave Recent Year
2004
Geometry Recent Year
2009
Emat Recent Year
2009
Other Recent Year
2009
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1994
Hydrtst Most Rcnt Pressure
1250
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D**** R* S*****
Preparer Title
Pipeline Safety Advisor
Preparer Email
D*************@e*********.com
Preparer Telephone
8326247531
Prepared Date
2020-03-30 00:00:00
Authorizer Name
C******* B* H********
Authorizer Telephone
832-624-7920
Authorizer Title
Empco Sshe Manager
Authorizer Email
C*******************@e*********.com
Narrative
When the release was discovered it did not appear that notification to the nrc would be required, however due to the location and logistics of transporting personnel and equipment to the site it was determined that the $50,000 criteria would be met. An nrc report was made at that time. Propane was bubbling through standing water in a low area, no sheen, emulsion or other visible water impact was observed during the release. [requested update 3/24/2020: release investigation determined it was seam weep from a penetrator-type lack of fusion at the seam (seam crack). This feature was repaired on november 7, 2013 by installation of a plidco clamp and recoating the pipe with type 2 wax tape.]
Report Received Date 2013-12-03 00:00:00
Iyear 2013
Report Number 20130386
Supplemental Number 33537
Report Type Supplemental Final
Operator Id 12624 PHMSA Enforcement
Name Mobil Corp
Operator Street Address 22777 Springwoods Village Parkway
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2013-11-03 13:50:00
Location Latitude 30.13945 Google Maps OpenStreetMap
Location Longitude -94.604717 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 1.2
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2013-11-03 18:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-11-03 20:38:00
Restart Datetime 2013-11-08 08:00:00
On Site Datetime 2013-11-03 18:00:00
Nrc Rpt Datetime 2013-11-04 09:15:00
Nrc Rpt Num 1064801 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Mr-114 Propane
Segment Name Hull To Beaumont
Onshore State Abbreviation Tx
Onshore Postal Code 77564
Onshore City Name Hull
Onshore County Name Hardin
Designated Location Survey Station No.
Designated Name 95+25
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 16
Pipe Wall Thickness 0.25
Pipe Smys 46000
Pipe Specification X-46
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Republic
Pipe Coating Type Coal Tar
Installation Year 1958
Manufactured Year 1958
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 58000
Est Cost Emergency 30000
Est Cost Environmental 0
Est Cost Other 0
Prpty 88100
Accident Psig 498
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 87900
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was a small leak, there were no alarms or controlroom information that indicated a leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Field Exam Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Seam Crack
Additional Crack Ind Yes
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Emat Ind Yes
Axial Recent Year 2009
Circ Wave Recent Year 2004
Geometry Recent Year 2009
Emat Recent Year 2009
Other Recent Year 2009
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1994
Hydrtst Most Rcnt Pressure 1250
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name D**** R* S*****
Preparer Title Pipeline Safety Advisor
Preparer Email D*************@e*********.com
Preparer Telephone 8326247531
Prepared Date 2020-03-30 00:00:00
Authorizer Name C******* B* H********
Authorizer Telephone 832-624-7920
Authorizer Title Empco Sshe Manager
Authorizer Email C*******************@e*********.com
Narrative When the release was discovered it did not appear that notification to the nrc would be required, however due to the location and logistics of transporting personnel and equipment to the site it was determined that the $50,000 criteria would be met. An nrc report was made at that time. Propane was bubbling through standing water in a low area, no sheen, emulsion or other visible water impact was observed during the release. [requested update 3/24/2020: release investigation determined it was seam weep from a penetrator-type lack of fusion at the seam (seam crack). This feature was repaired on november 7, 2013 by installation of a plidco clamp and recoating the pipe with type 2 wax tape.]

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