HL incident on 2013-11-03 — TX

Operator
Enbridge Pipelines (North Dakota) Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-11-03 14:08
Report number
Location
TX
Narrative
On saturday (11/02/13), two enbridge employees were working on valve maintenance, with a focus on draining water before freeze-up. Operators were working on the suction manifold of the berthold classic near mv311. One of the operators admittedly forgot to close a body bleed valve, which was utilized to relive pressure and speed up the draining process. Operators stated they finished this valve maintenance at approximately 1:00 p.M. On saturday november 2nd. On sunday (11/03/13), a contract site inspector noticed a petroleum odor coming from the east side of the terminal, he went over to inspect and found oil had sprayed and leaked on to the ground. He immediately notified the area supervisor. Upon receiving notification of the occurrence, the area supervisor notified the estevan control center to shut down the line. He then notified the sr. Manager of operations. Operator who left valve open was sent for post-accident drug and alcohol testing. Protocol for notifications, for all internal and external stakeholders, was completed within prescribed requirements. Cleanup of surface oil and contaminated soil via hydro excavating was started and completed. The emergency response process operated under the ics and was documented with an ics 201 packet. Contractors were utilitized to assist enbridge responders with product clean up and repair. Site cleanup and response commenced at approximately 4:00 p.M. On sunday (11/03/13). A total amount released and recovered was 9 barrels. Approximately 150 cubic yards of contaminated soil was hauled to an approved disposal facility. As requested by PHMSA, the time and date of the accident was changed to the time/date mv311 was opened by the control center. This is a speculated time of release that was not witnessed or visually verified. Actual discovery of the release did not occur until the following day when operations arrived on site. The ncr call was made following this visual confirmation.
Detailed record list
Report Received Date
2013-11-26 00:00:00
Iyear
2013
Report Number
20130380
Supplemental Number
19564
Report Type
Supplemental Final
Operator Id
Name
Enbridge Pipelines (North Dakota) Llc
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2013-11-02 17:47:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
9
Recovered Bbls
9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-11-03 14:08:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-11-03 14:17:00
Restart Datetime
2013-11-04 07:53:00
On Site Datetime
2013-11-03 14:08:00
Nrc Rpt Datetime
2013-11-03 15:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Berthold Station
Onshore State Abbreviation
Nd
Onshore Postal Code
58718
Onshore City Name
Berthold
Onshore County Name
Ward
Designated Location
Milepost/valve Station
Designated Name
24
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Other
Valve Mainline Details
Tank Suction Manifold Valve
Valve Manufacturer
Western (Dan-Ex)
Installation Year
2012
Manufactured Year
2012
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Bleed Valve Left Open During Maintenance Operations.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
900
Est Cost Prop Damage
0
Est Cost Emergency
235845
Est Cost Environmental
138386
Est Cost Other
0
Prpty
375131
Accident Psig
10
Mop Psig
270
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was an operator error as maintenance was performed on a valve and a bleed was left open.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
V****** L****
Preparer Title
Compliance Coordinator
Preparer Email
V************@e*******.com
Preparer Telephone
701-857-0857
Preparer Fax
701-857-0809
Prepared Date
2014-07-11 00:00:00
Authorizer Name
K**** G****
Authorizer Telephone
701-857-0880
Authorizer Title
Manager Support Services
Authorizer Email
K**********@e*******.com
Narrative
On saturday (11/02/13), two enbridge employees were working on valve maintenance, with a focus on draining water before freeze-up. Operators were working on the suction manifold of the berthold classic near mv311. One of the operators admittedly forgot to close a body bleed valve, which was utilized to relive pressure and speed up the draining process. Operators stated they finished this valve maintenance at approximately 1:00 p.M. On saturday november 2nd. On sunday (11/03/13), a contract site inspector noticed a petroleum odor coming from the east side of the terminal, he went over to inspect and found oil had sprayed and leaked on to the ground. He immediately notified the area supervisor. Upon receiving notification of the occurrence, the area supervisor notified the estevan control center to shut down the line. He then notified the sr. Manager of operations. Operator who left valve open was sent for post-accident drug and alcohol testing. Protocol for notifications, for all internal and external stakeholders, was completed within prescribed requirements. Cleanup of surface oil and contaminated soil via hydro excavating was started and completed. The emergency response process operated under the ics and was documented with an ics 201 packet. Contractors were utilitized to assist enbridge responders with product clean up and repair. Site cleanup and response commenced at approximately 4:00 p.M. On sunday (11/03/13). A total amount released and recovered was 9 barrels. Approximately 150 cubic yards of contaminated soil was hauled to an approved disposal facility. As requested by PHMSA, the time and date of the accident was changed to the time/date mv311 was opened by the control center. This is a speculated time of release that was not witnessed or visually verified. Actual discovery of the release did not occur until the following day when operations arrived on site. The ncr call was made following this visual confirmation.
Report Received Date 2013-11-26 00:00:00
Iyear 2013
Report Number 20130380
Supplemental Number 19564
Report Type Supplemental Final
Operator Id 15774 PHMSA Enforcement
Name Enbridge Pipelines (North Dakota) Llc
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2013-11-02 17:47:00
Location Latitude 48.325686 Google Maps OpenStreetMap
Location Longitude -101.752403 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 9
Recovered Bbls 9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2013-11-03 14:08:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-11-03 14:17:00
Restart Datetime 2013-11-04 07:53:00
On Site Datetime 2013-11-03 14:08:00
Nrc Rpt Datetime 2013-11-03 15:30:00
Nrc Rpt Num 1064762 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Berthold Station
Onshore State Abbreviation Nd
Onshore Postal Code 58718
Onshore City Name Berthold
Onshore County Name Ward
Designated Location Milepost/valve Station
Designated Name 24
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Other
Valve Mainline Details Tank Suction Manifold Valve
Valve Manufacturer Western (Dan-Ex)
Installation Year 2012
Manufactured Year 2012
Material Involved Carbon Steel
Release Type Other
Release Type Details Bleed Valve Left Open During Maintenance Operations.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 900
Est Cost Prop Damage 0
Est Cost Emergency 235845
Est Cost Environmental 138386
Est Cost Other 0
Prpty 375131
Accident Psig 10
Mop Psig 270
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function =< 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was an operator error as maintenance was performed on a valve and a bleed was left open.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name V****** L****
Preparer Title Compliance Coordinator
Preparer Email V************@e*******.com
Preparer Telephone 701-857-0857
Preparer Fax 701-857-0809
Prepared Date 2014-07-11 00:00:00
Authorizer Name K**** G****
Authorizer Telephone 701-857-0880
Authorizer Title Manager Support Services
Authorizer Email K**********@e*******.com
Narrative On saturday (11/02/13), two enbridge employees were working on valve maintenance, with a focus on draining water before freeze-up. Operators were working on the suction manifold of the berthold classic near mv311. One of the operators admittedly forgot to close a body bleed valve, which was utilized to relive pressure and speed up the draining process. Operators stated they finished this valve maintenance at approximately 1:00 p.M. On saturday november 2nd. On sunday (11/03/13), a contract site inspector noticed a petroleum odor coming from the east side of the terminal, he went over to inspect and found oil had sprayed and leaked on to the ground. He immediately notified the area supervisor. Upon receiving notification of the occurrence, the area supervisor notified the estevan control center to shut down the line. He then notified the sr. Manager of operations. Operator who left valve open was sent for post-accident drug and alcohol testing. Protocol for notifications, for all internal and external stakeholders, was completed within prescribed requirements. Cleanup of surface oil and contaminated soil via hydro excavating was started and completed. The emergency response process operated under the ics and was documented with an ics 201 packet. Contractors were utilitized to assist enbridge responders with product clean up and repair. Site cleanup and response commenced at approximately 4:00 p.M. On sunday (11/03/13). A total amount released and recovered was 9 barrels. Approximately 150 cubic yards of contaminated soil was hauled to an approved disposal facility. As requested by PHMSA, the time and date of the accident was changed to the time/date mv311 was opened by the control center. This is a speculated time of release that was not witnessed or visually verified. Actual discovery of the release did not occur until the following day when operations arrived on site. The ncr call was made following this visual confirmation.

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