HL incident on 2013-11-03 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10
Incident datetime
2013-11-03 02:20
Report number
Location
OK
Narrative
At approximately 02:20 hours on 11/03/2013 plant operators discovered a packing leak on the oneok northline #1 control valve. The control valve was isolated and product was blown down through the vapor recovery system of the medford fractionator. Valve packing on the control valve was repaired with new packing and pipeline was made ready for service. The pipeline was not running at the time. Control valve was installed proir to 2000.
Detailed record list
Report Received Date
2013-11-26 00:00:00
Iyear
2013
Report Number
20130376
Supplemental Number
19099
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2013-11-03 02:20:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
2.8
Intentional Release Bbls
2.8
Recovered Bbls
2.8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-11-03 02:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Down At Time Of Discovery
On Site Datetime
2013-11-03 02:20:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Medford Yard. North Line #1 Control Valve
Segment Name
Index 10127
Onshore State Abbreviation
Ok
Onshore Postal Code
73759
Onshore City Name
Medford
Onshore County Name
Grant
Designated Location
Milepost/valve Station
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
10
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
160
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
N*** J****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2014-03-07 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
At approximately 02:20 hours on 11/03/2013 plant operators discovered a packing leak on the oneok northline #1 control valve. The control valve was isolated and product was blown down through the vapor recovery system of the medford fractionator. Valve packing on the control valve was repaired with new packing and pipeline was made ready for service. The pipeline was not running at the time. Control valve was installed proir to 2000.
Report Received Date 2013-11-26 00:00:00
Iyear 2013
Report Number 20130376
Supplemental Number 19099
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2013-11-03 02:20:00
Location Latitude 36.775556 Google Maps OpenStreetMap
Location Longitude -97.755756 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 2.8
Intentional Release Bbls 2.8
Recovered Bbls 2.8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2013-11-03 02:20:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Down At Time Of Discovery
On Site Datetime 2013-11-03 02:20:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oneok Medford Yard. North Line #1 Control Valve
Segment Name Index 10127
Onshore State Abbreviation Ok
Onshore Postal Code 73759
Onshore City Name Medford
Onshore County Name Grant
Designated Location Milepost/valve Station
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Meter/prover
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 150
Est Cost Prop Damage 10
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 160
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Preparer Name N*** J****
Preparer Title Regulatory Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2014-03-07 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative At approximately 02:20 hours on 11/03/2013 plant operators discovered a packing leak on the oneok northline #1 control valve. The control valve was isolated and product was blown down through the vapor recovery system of the medford fractionator. Valve packing on the control valve was repaired with new packing and pipeline was made ready for service. The pipeline was not running at the time. Control valve was installed proir to 2000.

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