Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-11-03 — OK
Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$10
Incident datetime
2013-11-03 02:20
Report number
Location
OK
Narrative
At approximately 02:20 hours on 11/03/2013 plant operators discovered a packing leak on the oneok northline #1 control valve. The control valve was isolated and product was blown down through the vapor recovery system of the medford fractionator. Valve packing on the control valve was repaired with new packing and pipeline was made ready for service. The pipeline was not running at the time. Control valve was installed proir to 2000.
Detailed record list
Report Received Date
2013-11-26 00:00:00
Iyear
2013
Report Number
20130376
Supplemental Number
19099
Report Type
Supplemental Final
Operator Id
32109
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2013-11-03 02:20:00
Location Latitude
36.775556
Location Longitude
-97.755756
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
2.8
Intentional Release Bbls
2.8
Recovered Bbls
2.8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-11-03 02:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Down At Time Of Discovery
On Site Datetime
2013-11-03 02:20:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Medford Yard. North Line #1 Control Valve
Segment Name
Index 10127
Onshore State Abbreviation
Ok
Onshore Postal Code
73759
Onshore City Name
Medford
Onshore County Name
Grant
Designated Location
Milepost/valve Station
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
10
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
160
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
N*** J****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2014-03-07 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
At approximately 02:20 hours on 11/03/2013 plant operators discovered a packing leak on the oneok northline #1 control valve. The control valve was isolated and product was blown down through the vapor recovery system of the medford fractionator. Valve packing on the control valve was repaired with new packing and pipeline was made ready for service. The pipeline was not running at the time. Control valve was installed proir to 2000.
| Report Received Date | 2013-11-26 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130376 |
| Supplemental Number | 19099 |
| Report Type | Supplemental Final |
| Operator Id | 32109 PHMSA Enforcement |
| Name | Oneok Ngl Pipeline, Llc |
| Operator Street Address | 100 West Fifth Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2013-11-03 02:20:00 |
| Location Latitude | 36.775556 Google Maps OpenStreetMap |
| Location Longitude | -97.755756 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid) |
| Unintentional Release Bbls | 2.8 |
| Intentional Release Bbls | 2.8 |
| Recovered Bbls | 2.8 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2013-11-03 02:20:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Line Was Down At Time Of Discovery |
| On Site Datetime | 2013-11-03 02:20:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Oneok Medford Yard. North Line #1 Control Valve |
| Segment Name | Index 10127 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 73759 |
| Onshore City Name | Medford |
| Onshore County Name | Grant |
| Designated Location | Milepost/valve Station |
| Designated Name | 0+00 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Meter/prover |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 150 |
| Est Cost Prop Damage | 10 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 160 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Preparer Name | N*** J**** |
| Preparer Title | Regulatory Compliance Coordinator |
| Preparer Email | N*********@o****.com |
| Preparer Telephone | 580-395-6304 |
| Preparer Fax | 580-395-2933 |
| Prepared Date | 2014-03-07 00:00:00 |
| Authorizer Name | N*** J**** |
| Authorizer Telephone | 580-395-6304 |
| Authorizer Title | Regulatory Compliance Coordinator |
| Authorizer Email | N*********@o****.com |
| Narrative | At approximately 02:20 hours on 11/03/2013 plant operators discovered a packing leak on the oneok northline #1 control valve. The control valve was isolated and product was blown down through the vapor recovery system of the medford fractionator. Valve packing on the control valve was repaired with new packing and pipeline was made ready for service. The pipeline was not running at the time. Control valve was installed proir to 2000. |
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