HL incident on 2013-10-22 — TX

Operator
Rose Rock Midstream L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,300
Incident datetime
2013-10-22 12:29
Report number
Location
TX
Narrative
On october 22, 2013 at 12:29 pm air patrol services reported a spill on the garber to see 6" line. The line was immediately shutdown and emergency response personnel were dispatched to the location. Approximately 7 barrels of crude oil had escaped the pipeline due to an external corrosion pit located at the 5 o'clock position in the pipe. The area impacted was a plowed field. The oil had impacted an area approximately 75 yard wide and 75 yards in length. The pipeline was excavated and a temporary clamp was installed. The pipeline remained out of service until the following day. Impacted soils were removed to see station for remediation.
Detailed record list
Report Received Date
2013-11-22 00:00:00
Iyear
2013
Report Number
20130374
Supplemental Number
18802
Report Type
Supplemental
Operator Id
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-10-22 12:29:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
7
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-10-22 12:29:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-10-22 12:30:00
Restart Datetime
2013-10-23 08:00:00
On Site Datetime
2013-10-22 13:30:00
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Garber To See
Segment Name
Garber To See 6 Inch
Onshore State Abbreviation
Ok
Onshore Postal Code
74630
Onshore City Name
Billings
Onshore County Name
Noble
Designated Location
Milepost/valve Station
Designated Name
4.5
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6.625
Pipe Wall Thickness
0.28
Pipe Smys
35000
Pipe Specification
5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
None
Installation Year
1922
Manufactured Year
1922
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
700
Est Cost Prop Damage
2300
Est Cost Emergency
7000
Est Cost Environmental
0
Est Cost Other
0
Prpty
10000
Accident Psig
377
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
37488
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak too small to be identified by control room
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1960
Shielding Evident
No
Cathodic Survey Type
No
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
E*** N********
Preparer Title
District Supervisor
Preparer Email
E*********@s***********.com
Preparer Telephone
9182257758
Preparer Fax
9182252579
Prepared Date
2013-12-08 00:00:00
Authorizer Name
E**** C***
Authorizer Telephone
9185247143
Authorizer Title
Director Ehs
Authorizer Email
E****@s***********.com
Narrative
On october 22, 2013 at 12:29 pm air patrol services reported a spill on the garber to see 6" line. The line was immediately shutdown and emergency response personnel were dispatched to the location. Approximately 7 barrels of crude oil had escaped the pipeline due to an external corrosion pit located at the 5 o'clock position in the pipe. The area impacted was a plowed field. The oil had impacted an area approximately 75 yard wide and 75 yards in length. The pipeline was excavated and a temporary clamp was installed. The pipeline remained out of service until the following day. Impacted soils were removed to see station for remediation.
Report Received Date 2013-11-22 00:00:00
Iyear 2013
Report Number 20130374
Supplemental Number 18802
Report Type Supplemental
Operator Id 31476 PHMSA Enforcement
Name Rose Rock Midstream L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-10-22 12:29:00
Location Latitude 36.4302 Google Maps OpenStreetMap
Location Longitude -97.45631 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 7
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2013-10-22 12:29:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-10-22 12:30:00
Restart Datetime 2013-10-23 08:00:00
On Site Datetime 2013-10-22 13:30:00
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Garber To See
Segment Name Garber To See 6 Inch
Onshore State Abbreviation Ok
Onshore Postal Code 74630
Onshore City Name Billings
Onshore County Name Noble
Designated Location Milepost/valve Station
Designated Name 4.5
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6.625
Pipe Wall Thickness 0.28
Pipe Smys 35000
Pipe Specification 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type None
Installation Year 1922
Manufactured Year 1922
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 700
Est Cost Prop Damage 2300
Est Cost Emergency 7000
Est Cost Environmental 0
Est Cost Other 0
Prpty 10000
Accident Psig 377
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 37488
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak too small to be identified by control room
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1960
Shielding Evident No
Cathodic Survey Type No
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name E*** N********
Preparer Title District Supervisor
Preparer Email E*********@s***********.com
Preparer Telephone 9182257758
Preparer Fax 9182252579
Prepared Date 2013-12-08 00:00:00
Authorizer Name E**** C***
Authorizer Telephone 9185247143
Authorizer Title Director Ehs
Authorizer Email E****@s***********.com
Narrative On october 22, 2013 at 12:29 pm air patrol services reported a spill on the garber to see 6" line. The line was immediately shutdown and emergency response personnel were dispatched to the location. Approximately 7 barrels of crude oil had escaped the pipeline due to an external corrosion pit located at the 5 o'clock position in the pipe. The area impacted was a plowed field. The oil had impacted an area approximately 75 yard wide and 75 yards in length. The pipeline was excavated and a temporary clamp was installed. The pipeline remained out of service until the following day. Impacted soils were removed to see station for remediation.

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