Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-10-18 — TX
Operator
Holly Energy Partners - Operating, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$50
Incident datetime
2013-10-18 06:45
Report number
Location
TX
Narrative
Holly energy partners (hep) control center received a vapor alarm on the 8' beeson to lovington mainline pump (intrastate asset) and an hep field technician was dispatched to go on-site for a confirmatory check. The hep controller shut down the pump and isolated the pipeline. An hep contractor working on-site called an hep field technician and reported the release and the hep field technician called in the release to the control center. The majority of the free product was contained within the parameters of the hep facility and the free product that migrated outside of the facility was still contained on the company's right of way. Holly energy partners incident response resources completed the initial site clean-up the day of the incident; however, soil remediation efforts are on-going.
Detailed record list
Report Received Date
2013-11-15 00:00:00
Iyear
2013
Report Number
20130369
Supplemental Number
18736
Report Type
Supplemental Final
Operator Id
32011
Name
Holly Energy Partners - Operating, L.p.
Operator Street Address
2323 Victory Ave. Suite 1400
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75219
Local Datetime
2013-10-18 06:45:00
Location Latitude
32.782062
Location Longitude
-103.960134
Commodity Released Type
Crude Oil
Unintentional Release Bbls
20
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2013-10-18 06:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-10-18 07:20:00
Restart Datetime
2013-10-18 10:25:00
On Site Datetime
2013-10-18 07:40:00
Nrc Rpt Datetime
2013-10-18 08:43:00
Nrc Rpt Num
1063349
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Beeson Station
Segment Name
8" Beeson Mainline
Onshore State Abbreviation
Nm
Onshore Postal Code
88210
Onshore City Name
Artesia
Onshore County Name
Eddy
Federal
Yes
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
2009
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
2000
Est Cost Prop Damage
50
Est Cost Emergency
4000
Est Cost Environmental
20000
Est Cost Other
0
Prpty
26050
Accident Psig
769
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest Incorrect Action Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Other
Other Pump Details
Stainless Steel Tubing To The Bearing Cooler
Additional Vibration Ind
Yes
Preparer Name
S****** E*******
Preparer Title
Sr. Regulatory Coordinator
Preparer Email
S***************@h**********.com
Preparer Telephone
575-748-8943
Preparer Fax
214-540-1325
Prepared Date
2013-11-15 00:00:00
Authorizer Name
S****** E*******
Authorizer Telephone
575-748-8943
Authorizer Title
Sr. Regulatory Coordinator
Authorizer Email
S***************@h**********.com
Narrative
Holly energy partners (hep) control center received a vapor alarm on the 8' beeson to lovington mainline pump (intrastate asset) and an hep field technician was dispatched to go on-site for a confirmatory check. The hep controller shut down the pump and isolated the pipeline. An hep contractor working on-site called an hep field technician and reported the release and the hep field technician called in the release to the control center. The majority of the free product was contained within the parameters of the hep facility and the free product that migrated outside of the facility was still contained on the company's right of way. Holly energy partners incident response resources completed the initial site clean-up the day of the incident; however, soil remediation efforts are on-going.
| Report Received Date | 2013-11-15 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130369 |
| Supplemental Number | 18736 |
| Report Type | Supplemental Final |
| Operator Id | 32011 PHMSA Enforcement |
| Name | Holly Energy Partners - Operating, L.p. |
| Operator Street Address | 2323 Victory Ave. Suite 1400 |
| Operator City Name | Dallas |
| Operator State Abbreviation | TX |
| Operator Postal Code | 75219 |
| Local Datetime | 2013-10-18 06:45:00 |
| Location Latitude | 32.782062 Google Maps OpenStreetMap |
| Location Longitude | -103.960134 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 20 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations) |
| Incident Identified Datetime | 2013-10-18 06:45:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2013-10-18 07:20:00 |
| Restart Datetime | 2013-10-18 10:25:00 |
| On Site Datetime | 2013-10-18 07:40:00 |
| Nrc Rpt Datetime | 2013-10-18 08:43:00 |
| Nrc Rpt Num | 1063349 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Beeson Station |
| Segment Name | 8" Beeson Mainline |
| Onshore State Abbreviation | Nm |
| Onshore Postal Code | 88210 |
| Onshore City Name | Artesia |
| Onshore County Name | Eddy |
| Federal | Yes |
| Location Type | Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Pump |
| Installation Year | 2009 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Stainless |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | Yes |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 2000 |
| Est Cost Prop Damage | 50 |
| Est Cost Emergency | 4000 |
| Est Cost Environmental | 20000 |
| Est Cost Other | 0 |
| Prpty | 26050 |
| Accident Psig | 769 |
| Mop Psig | 1440 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | Yes |
| Cpm In Place Ind | No |
| Investigation Status | Yes, specify investigation result(s): (select all that apply) |
| Invest Schedule Ind | Yes |
| Invest No Control Room Ind | Yes |
| Invest Incorrect Action Ind | Yes |
| Employee Drug Test Ind | Yes |
| Contractor Drug Test Ind | No |
| Num Employees Tested | 1 |
| Num Employees Failed | 0 |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Other Pump Ind | Other |
| Other Pump Details | Stainless Steel Tubing To The Bearing Cooler |
| Additional Vibration Ind | Yes |
| Preparer Name | S****** E******* |
| Preparer Title | Sr. Regulatory Coordinator |
| Preparer Email | S***************@h**********.com |
| Preparer Telephone | 575-748-8943 |
| Preparer Fax | 214-540-1325 |
| Prepared Date | 2013-11-15 00:00:00 |
| Authorizer Name | S****** E******* |
| Authorizer Telephone | 575-748-8943 |
| Authorizer Title | Sr. Regulatory Coordinator |
| Authorizer Email | S***************@h**********.com |
| Narrative | Holly energy partners (hep) control center received a vapor alarm on the 8' beeson to lovington mainline pump (intrastate asset) and an hep field technician was dispatched to go on-site for a confirmatory check. The hep controller shut down the pump and isolated the pipeline. An hep contractor working on-site called an hep field technician and reported the release and the hep field technician called in the release to the control center. The majority of the free product was contained within the parameters of the hep facility and the free product that migrated outside of the facility was still contained on the company's right of way. Holly energy partners incident response resources completed the initial site clean-up the day of the incident; however, soil remediation efforts are on-going. |
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