HL incident on 2013-10-14 — TX

Operator
Mobil Pacific Pipeline Co
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$53,000
Incident datetime
2013-10-14 15:13
Report number
Location
TX
Narrative
A crude oil spill was reported to houston occ control center in close proximity of m 131 (thums) pipeline near pier d street, port of long beach, california. (the pipeline is in the street at this location) there are several pipeline operators within the same general area. Empco immediately shut down the thums pipeline system and isolated the leak section by utilizing motor operated valves. Empco company responded and company orso emergency response contractors were on site. (orso) response contractor is same for other pipeline operators within the same leak area. The leak was not identified to be empco, s until empco line was excavated and pin whole leak was found. The california state fire marshall (csfm) personnel were on site during excavation and repair of line. The pipeline excavation began on 10-14-13 and a (external corrosion) pin whole leak was found on 10-15-13. A temporary clamp was installed on 10-15-13 and line remained down until permanent repair was completed. A permanent repair was complete by replacing a new section of pipe on 10-18-13. The pipeline was restarted on 10-25-2013. 3-6-14 supplemental report created to add (pipe body) to part c question 3 missing data
Detailed record list
Report Received Date
2013-11-13 00:00:00
Iyear
2013
Report Number
20130364
Supplemental Number
19994
Report Type
Supplemental Final
Operator Id
Name
Mobil Pacific Pipeline Co
Operator Street Address
22777 Springwoods Village Parkway E3.5a.608
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2013-10-14 14:28:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6
Recovered Bbls
6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Thums Facility-(Third Party) Notified Houston Operation Control Center
Incident Identified Datetime
2013-10-14 15:13:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-10-14 14:28:00
Restart Datetime
2013-10-25 08:00:00
On Site Datetime
2013-10-14 15:13:00
Nrc Rpt Datetime
2013-10-14 16:06:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Thums Crude M142 Csfm Id-200 Port Of La Area
Segment Name
Thums M-142/122/89/119/131
Onshore State Abbreviation
Ca
Onshore Postal Code
90802
Onshore City Name
Long Beach
Onshore County Name
Los Angeles
Designated Location
Milepost/valve Station
Designated Name
Thums-Gaylord
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
54
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10.75
Pipe Wall Thickness
0.25
Pipe Smys
52000
Pipe Specification
5lx-52
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
T-2 Wrap & Polyken Tape Wrap
Installation Year
1968
Manufactured Year
1968
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
600
Est Cost Prop Damage
53000
Est Cost Emergency
85000
Est Cost Environmental
227000
Est Cost Other
0
Est Cost Other Details
Remediation Work Still In Progress.
Prpty
365600
Accident Psig
674
Mop Psig
780
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
21101
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller action was not a factor. The leak was caused by external corrosion.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Other Corrosion Ind
Yes
Corrosion Type Details
Direct Result From Of Improper Field Applied Coating From The Bend To The Straight Pipe
Field Exam Basis Ind
Yes
Other Basis Ind
Yes
Corrosion Basis Details
Improper Field Coating In Original Construction In Field Wrap In 1968 -T-2 Coating Applied At Transition Of Mill Coating. Improper Field Applied Polyken Tape Wrap Near Pipe Bend.
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1979
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2013
Prior Damage
Yes
Collected Data Ind
Yes
Ultrasonic Ind
Yes
Ultrasonic Recent Year
2011
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2013
Hydrtst Most Rcnt Pressure
980
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
L**** E H********
Preparer Title
Pipeline Safety Advisor
Preparer Email
L****************@e*********.com
Preparer Telephone
903-654-5345
Preparer Fax
903-654-5374
Prepared Date
2014-12-18 00:00:00
Authorizer Name
J**** B R***
Authorizer Telephone
713-656-0227
Authorizer Title
She-Safety Health Environmental Manager
Authorizer Email
J***********@e*********.com
Narrative
A crude oil spill was reported to houston occ control center in close proximity of m 131 (thums) pipeline near pier d street, port of long beach, california. (the pipeline is in the street at this location) there are several pipeline operators within the same general area. Empco immediately shut down the thums pipeline system and isolated the leak section by utilizing motor operated valves. Empco company responded and company orso emergency response contractors were on site. (orso) response contractor is same for other pipeline operators within the same leak area. The leak was not identified to be empco, s until empco line was excavated and pin whole leak was found. The california state fire marshall (csfm) personnel were on site during excavation and repair of line. The pipeline excavation began on 10-14-13 and a (external corrosion) pin whole leak was found on 10-15-13. A temporary clamp was installed on 10-15-13 and line remained down until permanent repair was completed. A permanent repair was complete by replacing a new section of pipe on 10-18-13. The pipeline was restarted on 10-25-2013. 3-6-14 supplemental report created to add (pipe body) to part c question 3 missing data
Report Received Date 2013-11-13 00:00:00
Iyear 2013
Report Number 20130364
Supplemental Number 19994
Report Type Supplemental Final
Operator Id 30005 PHMSA Enforcement
Name Mobil Pacific Pipeline Co
Operator Street Address 22777 Springwoods Village Parkway E3.5a.608
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2013-10-14 14:28:00
Location Latitude 33.769722 Google Maps OpenStreetMap
Location Longitude -118.208889 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 6
Recovered Bbls 6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Thums Facility-(Third Party) Notified Houston Operation Control Center
Incident Identified Datetime 2013-10-14 15:13:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-10-14 14:28:00
Restart Datetime 2013-10-25 08:00:00
On Site Datetime 2013-10-14 15:13:00
Nrc Rpt Datetime 2013-10-14 16:06:00
Nrc Rpt Num 1062999 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Thums Crude M142 Csfm Id-200 Port Of La Area
Segment Name Thums M-142/122/89/119/131
Onshore State Abbreviation Ca
Onshore Postal Code 90802
Onshore City Name Long Beach
Onshore County Name Los Angeles
Designated Location Milepost/valve Station
Designated Name Thums-Gaylord
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 54
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10.75
Pipe Wall Thickness 0.25
Pipe Smys 52000
Pipe Specification 5lx-52
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Other
Pipe Coating Details T-2 Wrap & Polyken Tape Wrap
Installation Year 1968
Manufactured Year 1968
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 600
Est Cost Prop Damage 53000
Est Cost Emergency 85000
Est Cost Environmental 227000
Est Cost Other 0
Est Cost Other Details Remediation Work Still In Progress.
Prpty 365600
Accident Psig 674
Mop Psig 780
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 21101
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller action was not a factor. The leak was caused by external corrosion.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Other Corrosion Ind Yes
Corrosion Type Details Direct Result From Of Improper Field Applied Coating From The Bend To The Straight Pipe
Field Exam Basis Ind Yes
Other Basis Ind Yes
Corrosion Basis Details Improper Field Coating In Original Construction In Field Wrap In 1968 -T-2 Coating Applied At Transition Of Mill Coating. Improper Field Applied Polyken Tape Wrap Near Pipe Bend.
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1979
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2013
Prior Damage Yes
Collected Data Ind Yes
Ultrasonic Ind Yes
Ultrasonic Recent Year 2011
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2013
Hydrtst Most Rcnt Pressure 980
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name L**** E H********
Preparer Title Pipeline Safety Advisor
Preparer Email L****************@e*********.com
Preparer Telephone 903-654-5345
Preparer Fax 903-654-5374
Prepared Date 2014-12-18 00:00:00
Authorizer Name J**** B R***
Authorizer Telephone 713-656-0227
Authorizer Title She-Safety Health Environmental Manager
Authorizer Email J***********@e*********.com
Narrative A crude oil spill was reported to houston occ control center in close proximity of m 131 (thums) pipeline near pier d street, port of long beach, california. (the pipeline is in the street at this location) there are several pipeline operators within the same general area. Empco immediately shut down the thums pipeline system and isolated the leak section by utilizing motor operated valves. Empco company responded and company orso emergency response contractors were on site. (orso) response contractor is same for other pipeline operators within the same leak area. The leak was not identified to be empco, s until empco line was excavated and pin whole leak was found. The california state fire marshall (csfm) personnel were on site during excavation and repair of line. The pipeline excavation began on 10-14-13 and a (external corrosion) pin whole leak was found on 10-15-13. A temporary clamp was installed on 10-15-13 and line remained down until permanent repair was completed. A permanent repair was complete by replacing a new section of pipe on 10-18-13. The pipeline was restarted on 10-25-2013. 3-6-14 supplemental report created to add (pipe body) to part c question 3 missing data

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