HL incident on 2013-09-23 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$141,500
Incident datetime
2013-09-23 22:50
Report number
Location
TX
Narrative
On 9/23/2013 a technician discovered a patch of dead vegetation on the pipeline row within the fence line of abilene station located near solomon, kansas in ottawa county. A subsequent survey of the area indicated lel was present. The pipeline was immediately shut down and the leaking segment was blocked in. Upon excavation, it was identified that the leak originated from a stopple fitting, around the completion plug and blind flange o-ring. Line pressure was lowered by reversing the line and flowing back into conway. Once the pressure was lowered, an attempt was made to blow down the stopple. Upon the unsuccessful attempt to blow down the stopple, it was determined that the stopple fitting would be cut out. The nrc was then notified as the estimated cost to repair was expected to exceed $50,000. The line segment from am 49 to abilene station was flared off, purged with nitrogen, the stopple cut out, and replaced with pipe. The pipeline was restarted on 9/28/2013. Preliminary field analysis conducted by operations determined the leak to be located (by visual observation) between the stopple fitting flange and the blind flange, indicating a possible o-ring failure. The leak location was determined using an lel monitor and snoop gas leak detector but the stopple was not disassembled. Lab analysis concluded there are two possible failure scenarios for the o-ring: 1) the o-ring was not properly seated when it was installed. A contributing factor may have been an improperly sized o-ring. 2) the o-ring blew out during service. Contributing factors may have been misalignment of the flanges, improper torque, degradation of the o-ring or an improper size.
Detailed record list
Report Received Date
2013-10-22 00:00:00
Iyear
2013
Report Number
20130342
Supplemental Number
21877
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-09-23 22:50:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
0.2
Intentional Release Bbls
1097
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-09-23 22:50:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-09-23 22:50:00
Restart Datetime
2013-09-28 15:39:00
On Site Datetime
2013-09-23 22:50:00
Nrc Rpt Datetime
2013-09-23 23:27:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
West Leg Mainline, Conway To Mankato
Segment Name
Lid 410
Onshore State Abbreviation
Ks
Onshore Postal Code
67480
Onshore City Name
Soloman
Onshore County Name
Ottawa
Designated Location
Milepost/valve Station
Designated Name
Abilene
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year
1989
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
10
Est Cost Prop Damage
141500
Est Cost Emergency
10000
Est Cost Environmental
0
Est Cost Other
0
Prpty
151510
Accident Psig
730
Mop Psig
1309
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
17000
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Other Ind
Yes
Operation Related Details
The Results Of The Metallurgical Analysis Indicated Two Possible Failure Scenarios For The O-Ring: 1) The O-Ring Was Not Properly Seated When It Was Installed. 2) The O-Ring Blew Out During Service.
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
R** L**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
R***@e****.com
Preparer Telephone
7133816741
Prepared Date
2016-11-21 00:00:00
Authorizer Name
R** L**
Authorizer Telephone
7133816741
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
R***@e****.com
Narrative
On 9/23/2013 a technician discovered a patch of dead vegetation on the pipeline row within the fence line of abilene station located near solomon, kansas in ottawa county. A subsequent survey of the area indicated lel was present. The pipeline was immediately shut down and the leaking segment was blocked in. Upon excavation, it was identified that the leak originated from a stopple fitting, around the completion plug and blind flange o-ring. Line pressure was lowered by reversing the line and flowing back into conway. Once the pressure was lowered, an attempt was made to blow down the stopple. Upon the unsuccessful attempt to blow down the stopple, it was determined that the stopple fitting would be cut out. The nrc was then notified as the estimated cost to repair was expected to exceed $50,000. The line segment from am 49 to abilene station was flared off, purged with nitrogen, the stopple cut out, and replaced with pipe. The pipeline was restarted on 9/28/2013. Preliminary field analysis conducted by operations determined the leak to be located (by visual observation) between the stopple fitting flange and the blind flange, indicating a possible o-ring failure. The leak location was determined using an lel monitor and snoop gas leak detector but the stopple was not disassembled. Lab analysis concluded there are two possible failure scenarios for the o-ring: 1) the o-ring was not properly seated when it was installed. A contributing factor may have been an improperly sized o-ring. 2) the o-ring blew out during service. Contributing factors may have been misalignment of the flanges, improper torque, degradation of the o-ring or an improper size.
Report Received Date 2013-10-22 00:00:00
Iyear 2013
Report Number 20130342
Supplemental Number 21877
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-09-23 22:50:00
Location Latitude 39.02942 Google Maps OpenStreetMap
Location Longitude -97.38027 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 0.2
Intentional Release Bbls 1097
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2013-09-23 22:50:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-09-23 22:50:00
Restart Datetime 2013-09-28 15:39:00
On Site Datetime 2013-09-23 22:50:00
Nrc Rpt Datetime 2013-09-23 23:27:00
Nrc Rpt Num 1061041 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name West Leg Mainline, Conway To Mankato
Segment Name Lid 410
Onshore State Abbreviation Ks
Onshore Postal Code 67480
Onshore City Name Soloman
Onshore County Name Ottawa
Designated Location Milepost/valve Station
Designated Name Abilene
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year 1989
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 10
Est Cost Prop Damage 141500
Est Cost Emergency 10000
Est Cost Environmental 0
Est Cost Other 0
Prpty 151510
Accident Psig 730
Mop Psig 1309
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 17000
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Other Ind Yes
Operation Related Details The Results Of The Metallurgical Analysis Indicated Two Possible Failure Scenarios For The O-Ring: 1) The O-Ring Was Not Properly Seated When It Was Installed. 2) The O-Ring Blew Out During Service.
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name R** L**
Preparer Title Pipeline Compliance Engineer
Preparer Email R***@e****.com
Preparer Telephone 7133816741
Prepared Date 2016-11-21 00:00:00
Authorizer Name R** L**
Authorizer Telephone 7133816741
Authorizer Title Pipeline Compliance Engineer
Authorizer Email R***@e****.com
Narrative On 9/23/2013 a technician discovered a patch of dead vegetation on the pipeline row within the fence line of abilene station located near solomon, kansas in ottawa county. A subsequent survey of the area indicated lel was present. The pipeline was immediately shut down and the leaking segment was blocked in. Upon excavation, it was identified that the leak originated from a stopple fitting, around the completion plug and blind flange o-ring. Line pressure was lowered by reversing the line and flowing back into conway. Once the pressure was lowered, an attempt was made to blow down the stopple. Upon the unsuccessful attempt to blow down the stopple, it was determined that the stopple fitting would be cut out. The nrc was then notified as the estimated cost to repair was expected to exceed $50,000. The line segment from am 49 to abilene station was flared off, purged with nitrogen, the stopple cut out, and replaced with pipe. The pipeline was restarted on 9/28/2013. Preliminary field analysis conducted by operations determined the leak to be located (by visual observation) between the stopple fitting flange and the blind flange, indicating a possible o-ring failure. The leak location was determined using an lel monitor and snoop gas leak detector but the stopple was not disassembled. Lab analysis concluded there are two possible failure scenarios for the o-ring: 1) the o-ring was not properly seated when it was installed. A contributing factor may have been an improperly sized o-ring. 2) the o-ring blew out during service. Contributing factors may have been misalignment of the flanges, improper torque, degradation of the o-ring or an improper size.

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