HL incident on 2013-09-17 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$194,000
Incident datetime
2013-09-17 02:06
Report number
Location
TX
Narrative
On 9/17/2013, a third party operator notified enterprise pipeline control of an ice ball on the 10" south leg loop line valve. An enterprise technician was dispatched and confirmed a pin hole leak on the valve body. The pipeline was not running at the time. Two valves were closed to block the leaking segment and flares were set up to displace the line. Once displaced, the leaking valve was cut out and replaced with another valve. The line was returned to service on 9/26/2013 upon completion of the repairs. Metallurgical analysis identified the failure was caused by a poor quality weld repair. Weld defects that were observed include a small section of unmelted filler rod or wire that was inadvertently left in the weld, porosity, lack of fusion, mechanical notches, and severe gouging of the base metal. These conditions constituted latent defects that eventually resulted in crack propagation to failure and loss of containment. Note: the name plate on the valve identifies it was rebuilt in 1/17/1992 and the repair procedures and inspection records are not available.
Detailed record list
Report Received Date
2013-10-15 00:00:00
Iyear
2013
Report Number
20130338
Supplemental Number
21876
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-09-17 02:06:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane/propane Mix
Unintentional Release Bbls
4
Intentional Release Bbls
2200
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Pipeline Technician Working In The Area
Incident Identified Datetime
2013-09-17 02:06:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Not Running At The Time.
On Site Datetime
2013-09-17 02:06:00
Nrc Rpt Datetime
2013-09-17 03:01:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
South Leg Loop
Segment Name
Lid 220
Onshore State Abbreviation
Tx
Onshore Postal Code
79081
Onshore City Name
Waka
Onshore County Name
Ochiltree
Designated Location
Milepost/valve Station
Designated Name
Spearman
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Grove
Installation Year
1971
Manufactured Year
1971
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
40
Est Cost Prop Damage
194000
Est Cost Emergency
15000
Est Cost Environmental
0
Est Cost Other
7000
Est Cost Other Details
Lab Analysis Of Valve
Prpty
216040
Accident Psig
862
Mop Psig
1275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
31680
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Additional Other Ind
Yes
Eq Additional Other Details
The Failure Was Caused By A Poor Quality Weld Repair.
Preparer Name
R** L**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
R***@e****.com
Preparer Telephone
7133816741
Prepared Date
2016-11-21 00:00:00
Authorizer Name
R** L**
Authorizer Telephone
7133816741
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
R***@e****.com
Narrative
On 9/17/2013, a third party operator notified enterprise pipeline control of an ice ball on the 10" south leg loop line valve. An enterprise technician was dispatched and confirmed a pin hole leak on the valve body. The pipeline was not running at the time. Two valves were closed to block the leaking segment and flares were set up to displace the line. Once displaced, the leaking valve was cut out and replaced with another valve. The line was returned to service on 9/26/2013 upon completion of the repairs. Metallurgical analysis identified the failure was caused by a poor quality weld repair. Weld defects that were observed include a small section of unmelted filler rod or wire that was inadvertently left in the weld, porosity, lack of fusion, mechanical notches, and severe gouging of the base metal. These conditions constituted latent defects that eventually resulted in crack propagation to failure and loss of containment. Note: the name plate on the valve identifies it was rebuilt in 1/17/1992 and the repair procedures and inspection records are not available.
Report Received Date 2013-10-15 00:00:00
Iyear 2013
Report Number 20130338
Supplemental Number 21876
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-09-17 02:06:00
Location Latitude 36.086068 Google Maps OpenStreetMap
Location Longitude -101.046424 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane/propane Mix
Unintentional Release Bbls 4
Intentional Release Bbls 2200
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Pipeline Technician Working In The Area
Incident Identified Datetime 2013-09-17 02:06:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline Was Not Running At The Time.
On Site Datetime 2013-09-17 02:06:00
Nrc Rpt Datetime 2013-09-17 03:01:00
Nrc Rpt Num 1060390 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name South Leg Loop
Segment Name Lid 220
Onshore State Abbreviation Tx
Onshore Postal Code 79081
Onshore City Name Waka
Onshore County Name Ochiltree
Designated Location Milepost/valve Station
Designated Name Spearman
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Grove
Installation Year 1971
Manufactured Year 1971
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 40
Est Cost Prop Damage 194000
Est Cost Emergency 15000
Est Cost Environmental 0
Est Cost Other 7000
Est Cost Other Details Lab Analysis Of Valve
Prpty 216040
Accident Psig 862
Mop Psig 1275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 31680
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Additional Other Ind Yes
Eq Additional Other Details The Failure Was Caused By A Poor Quality Weld Repair.
Preparer Name R** L**
Preparer Title Pipeline Compliance Engineer
Preparer Email R***@e****.com
Preparer Telephone 7133816741
Prepared Date 2016-11-21 00:00:00
Authorizer Name R** L**
Authorizer Telephone 7133816741
Authorizer Title Pipeline Compliance Engineer
Authorizer Email R***@e****.com
Narrative On 9/17/2013, a third party operator notified enterprise pipeline control of an ice ball on the 10" south leg loop line valve. An enterprise technician was dispatched and confirmed a pin hole leak on the valve body. The pipeline was not running at the time. Two valves were closed to block the leaking segment and flares were set up to displace the line. Once displaced, the leaking valve was cut out and replaced with another valve. The line was returned to service on 9/26/2013 upon completion of the repairs. Metallurgical analysis identified the failure was caused by a poor quality weld repair. Weld defects that were observed include a small section of unmelted filler rod or wire that was inadvertently left in the weld, porosity, lack of fusion, mechanical notches, and severe gouging of the base metal. These conditions constituted latent defects that eventually resulted in crack propagation to failure and loss of containment. Note: the name plate on the valve identifies it was rebuilt in 1/17/1992 and the repair procedures and inspection records are not available.

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