HL incident on 2013-09-04 — TX

Operator
Nustar Logistics, L.p.
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$109,184
Incident datetime
2013-09-04 07:40
Report number
Location
TX
Narrative
On tuesday, september 3, 2013, nustar's control room in san antonio, tx received a low-suction alarm on nustar's 8-inch 53p three rivers to san antonio (south) pipeline system. The three rivers pump station was automatically shut down on the alarm, and the pump station discharge valve was closed. Throughout the evening of september 3rd and early morning of september 4th, nustar personnel drove the entire pipeline segment from three rivers, tx to nustar's san antonio south terminal checking immediate response areas. On wednesday, september 4, 2013, nustar personnel discovered a release on the row of the pipeline approximately 0.5 miles north of hwy 72 near three rivers, tx. The accident occurred in a rural, non-hca location in live oak county, tx. Approximately 2,752 barrels of gasoline was released, and approximately 817 barrels have been recovered to-date. The affected pipe segment was removed and replaced on thursday, september 5, 2013. The affected pipe segment was sent to a third party metallurgical laboratory for analysis. The rupture was caused by external corrosion underneath tape coating applied over the girth weld region. The corrosion was isolated to the pipe beneath the tape coating. The corrosion progressed to a depth where the remaining wall thickness was unable to contain the internal pressure.
Detailed record list
Report Received Date
2013-10-03 00:00:00
Iyear
2013
Report Number
20130332
Supplemental Number
18957
Report Type
Supplemental Final
Operator Id
Name
Nustar Logistics, L.p.
Operator Street Address
8111 Westchester Drive
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75225
Local Datetime
2013-09-03 21:34:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
2752
Recovered Bbls
817
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2013-09-04 07:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-09-03 21:34:00
Restart Datetime
2013-09-05 21:09:00
On Site Datetime
2013-09-04 07:40:00
Nrc Rpt Datetime
2013-09-04 07:57:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
53p-Three Rivers To San Antonio (South) Pl
Segment Name
Three Rivers To San Antonio South Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
78071
Onshore City Name
Three Rivers
Onshore County Name
Live Oak
Designated Location
Survey Station No.
Designated Name
222+34
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
54
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.219
Pipe Smys
52000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Dalmine
Pipe Coating Type
Cold Applied Tape
Installation Year
1979
Manufactured Year
1978
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Width
3.1
Rupture Length
14.3
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
1045900
Est Cost Gas Released
217560
Est Cost Prop Damage
109184
Est Cost Emergency
151051
Est Cost Environmental
200000
Est Cost Other
0
Prpty
1723695
Accident Psig
1742
Mop Psig
1865
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
48854
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The scada system responded automatically to the low-suction alarm. Nustar control room personnel recognized the event and responded appropriately.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1979
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2013
Close Interval Survey Year
2009
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2009
Geometry Recent Year
2009
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R****** P****
Preparer Title
Lead Pipeline Safety Specialist
Preparer Email
R************@n***********.com
Preparer Telephone
361-249-9417
Preparer Fax
210-918-7117
Prepared Date
2014-01-27 00:00:00
Authorizer Name
W** G***
Authorizer Telephone
361-249-9402
Authorizer Title
Vice President And General Manager Operations
Authorizer Email
W*******@n***********.com
Narrative
On tuesday, september 3, 2013, nustar's control room in san antonio, tx received a low-suction alarm on nustar's 8-inch 53p three rivers to san antonio (south) pipeline system. The three rivers pump station was automatically shut down on the alarm, and the pump station discharge valve was closed. Throughout the evening of september 3rd and early morning of september 4th, nustar personnel drove the entire pipeline segment from three rivers, tx to nustar's san antonio south terminal checking immediate response areas. On wednesday, september 4, 2013, nustar personnel discovered a release on the row of the pipeline approximately 0.5 miles north of hwy 72 near three rivers, tx. The accident occurred in a rural, non-hca location in live oak county, tx. Approximately 2,752 barrels of gasoline was released, and approximately 817 barrels have been recovered to-date. The affected pipe segment was removed and replaced on thursday, september 5, 2013. The affected pipe segment was sent to a third party metallurgical laboratory for analysis. The rupture was caused by external corrosion underneath tape coating applied over the girth weld region. The corrosion was isolated to the pipe beneath the tape coating. The corrosion progressed to a depth where the remaining wall thickness was unable to contain the internal pressure.
Report Received Date 2013-10-03 00:00:00
Iyear 2013
Report Number 20130332
Supplemental Number 18957
Report Type Supplemental Final
Operator Id 31454 PHMSA Enforcement
Name Nustar Logistics, L.p.
Operator Street Address 8111 Westchester Drive
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75225
Local Datetime 2013-09-03 21:34:00
Location Latitude 28.488488 Google Maps OpenStreetMap
Location Longitude -98.160559 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 2752
Recovered Bbls 817
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2013-09-04 07:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-09-03 21:34:00
Restart Datetime 2013-09-05 21:09:00
On Site Datetime 2013-09-04 07:40:00
Nrc Rpt Datetime 2013-09-04 07:57:00
Nrc Rpt Num 1059132 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name 53p-Three Rivers To San Antonio (South) Pl
Segment Name Three Rivers To San Antonio South Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 78071
Onshore City Name Three Rivers
Onshore County Name Live Oak
Designated Location Survey Station No.
Designated Name 222+34
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 54
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.219
Pipe Smys 52000
Pipe Specification Api 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Dalmine
Pipe Coating Type Cold Applied Tape
Installation Year 1979
Manufactured Year 1978
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Width 3.1
Rupture Length 14.3
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 1045900
Est Cost Gas Released 217560
Est Cost Prop Damage 109184
Est Cost Emergency 151051
Est Cost Environmental 200000
Est Cost Other 0
Prpty 1723695
Accident Psig 1742
Mop Psig 1865
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 48854
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The scada system responded automatically to the low-suction alarm. Nustar control room personnel recognized the event and responded appropriately.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1979
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2013
Close Interval Survey Year 2009
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2009
Geometry Recent Year 2009
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R****** P****
Preparer Title Lead Pipeline Safety Specialist
Preparer Email R************@n***********.com
Preparer Telephone 361-249-9417
Preparer Fax 210-918-7117
Prepared Date 2014-01-27 00:00:00
Authorizer Name W** G***
Authorizer Telephone 361-249-9402
Authorizer Title Vice President And General Manager Operations
Authorizer Email W*******@n***********.com
Narrative On tuesday, september 3, 2013, nustar's control room in san antonio, tx received a low-suction alarm on nustar's 8-inch 53p three rivers to san antonio (south) pipeline system. The three rivers pump station was automatically shut down on the alarm, and the pump station discharge valve was closed. Throughout the evening of september 3rd and early morning of september 4th, nustar personnel drove the entire pipeline segment from three rivers, tx to nustar's san antonio south terminal checking immediate response areas. On wednesday, september 4, 2013, nustar personnel discovered a release on the row of the pipeline approximately 0.5 miles north of hwy 72 near three rivers, tx. The accident occurred in a rural, non-hca location in live oak county, tx. Approximately 2,752 barrels of gasoline was released, and approximately 817 barrels have been recovered to-date. The affected pipe segment was removed and replaced on thursday, september 5, 2013. The affected pipe segment was sent to a third party metallurgical laboratory for analysis. The rupture was caused by external corrosion underneath tape coating applied over the girth weld region. The corrosion was isolated to the pipe beneath the tape coating. The corrosion progressed to a depth where the remaining wall thickness was unable to contain the internal pressure.

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