HL incident on 2013-09-04 — TX

Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-09-04 12:00
Report number
Location
TX
Narrative
A one barrel leak occurred on the discharge piping of an out of service gathering line pump. Leak contained to pump site area. Site was remediated, piping isolated and line segment blinded.
Detailed record list
Report Received Date
2013-10-03 00:00:00
Iyear
2013
Report Number
20130331
Supplemental Number
18630
Report Type
Original Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-09-04 12:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-09-04 12:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Occurred On Dead Leg Piping On The Discharge Of An Oos Pump Unit.
On Site Datetime
2013-09-04 12:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Thomason Pump Unit
Segment Name
Alex To Chitwood 3" & 4"-553016
Onshore State Abbreviation
Ok
Onshore Postal Code
73002
Onshore City Name
Alex
Onshore County Name
Grady
Designated Location
Survey Station No.
Designated Name
183+61
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
100
Est Cost Other
0
Prpty
200
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Specialist
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
281-637-6425
Prepared Date
2013-10-03 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Specialist
Authorizer Email
T*********@s**************.com
Narrative
A one barrel leak occurred on the discharge piping of an out of service gathering line pump. Leak contained to pump site area. Site was remediated, piping isolated and line segment blinded.
Report Received Date 2013-10-03 00:00:00
Iyear 2013
Report Number 20130331
Supplemental Number 18630
Report Type Original Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-09-04 12:00:00
Location Latitude 34.874565 Google Maps OpenStreetMap
Location Longitude -97.79908 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2013-09-04 12:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Leak Occurred On Dead Leg Piping On The Discharge Of An Oos Pump Unit.
On Site Datetime 2013-09-04 12:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Thomason Pump Unit
Segment Name Alex To Chitwood 3" & 4"-553016
Onshore State Abbreviation Ok
Onshore Postal Code 73002
Onshore City Name Alex
Onshore County Name Grady
Designated Location Survey Station No.
Designated Name 183+61
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Underground
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Release Type Leak
Leak Type Pinhole
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 100
Est Cost Other 0
Prpty 200
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Specialist
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 281-637-6425
Prepared Date 2013-10-03 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Specialist
Authorizer Email T*********@s**************.com
Narrative A one barrel leak occurred on the discharge piping of an out of service gathering line pump. Leak contained to pump site area. Site was remediated, piping isolated and line segment blinded.

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