Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-08-29 — OH
Operator
Marathon Pipe Line Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$92,500
Incident datetime
2013-08-29 07:34
Report number
Location
OH
Narrative
During a routine station check, freestanding crude oil was discovered in two excavations associated with recent project work at the station. The source of the release was identified as internal corrosion on dead leg piping near the manifold. The piping was removed along with 9.24 tons of soil.
Detailed record list
Report Received Date
2013-09-24 00:00:00
Iyear
2013
Report Number
20130328
Supplemental Number
20800
Report Type
Supplemental Final
Operator Id
32147
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2013-08-29 07:30:00
Location Latitude
39.3271159
Location Longitude
-87.8981323
Commodity Released Type
Crude Oil
Unintentional Release Bbls
273
Recovered Bbls
273
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-08-29 07:34:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-08-29 07:34:00
Restart Datetime
2013-08-31 00:19:00
On Site Datetime
2013-08-29 07:34:00
Nrc Rpt Datetime
2013-08-29 08:42:00
Nrc Rpt Num
1058582
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Martinsville Station
Segment Name
Patoka-Martinsville 20" And Martinsville-Lima 22"
Onshore State Abbreviation
Il
Onshore Postal Code
62442
Onshore City Name
Martinsville
Onshore County Name
Clark
Designated Location
Survey Station No.
Designated Name
Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Installation Year
2001
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
27095
Est Cost Prop Damage
92500
Est Cost Emergency
400000
Est Cost Environmental
0
Est Cost Other
0
Prpty
519595
Accident Psig
15
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
D******* S***
Preparer Title
Hes Professional
Preparer Email
D*****@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2015-10-06 00:00:00
Authorizer Name
R****** W* B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory And Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
During a routine station check, freestanding crude oil was discovered in two excavations associated with recent project work at the station. The source of the release was identified as internal corrosion on dead leg piping near the manifold. The piping was removed along with 9.24 tons of soil.
| Report Received Date | 2013-09-24 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130328 |
| Supplemental Number | 20800 |
| Report Type | Supplemental Final |
| Operator Id | 32147 PHMSA Enforcement |
| Name | Marathon Pipe Line Llc |
| Operator Street Address | 539 South Main Street |
| Operator City Name | Findlay |
| Operator State Abbreviation | OH |
| Operator Postal Code | 45840 |
| Local Datetime | 2013-08-29 07:30:00 |
| Location Latitude | 39.3271159 Google Maps OpenStreetMap |
| Location Longitude | -87.8981323 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 273 |
| Recovered Bbls | 273 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Contractor Working For The Operator |
| Incident Identified Datetime | 2013-08-29 07:34:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2013-08-29 07:34:00 |
| Restart Datetime | 2013-08-31 00:19:00 |
| On Site Datetime | 2013-08-29 07:34:00 |
| Nrc Rpt Datetime | 2013-08-29 08:42:00 |
| Nrc Rpt Num | 1058582 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Martinsville Station |
| Segment Name | Patoka-Martinsville 20" And Martinsville-Lima 22" |
| Onshore State Abbreviation | Il |
| Onshore Postal Code | 62442 |
| Onshore City Name | Martinsville |
| Onshore County Name | Clark |
| Designated Location | Survey Station No. |
| Designated Name | Facility |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 48 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Relief Line And Relief Equipment |
| Installation Year | 2001 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Other Pop Ind | Yes |
| Other Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 27095 |
| Est Cost Prop Damage | 92500 |
| Est Cost Emergency | 400000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 519595 |
| Accident Psig | 15 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | Yes, specify investigation result(s): (select all that apply) |
| Invest No Control Room Ind | Yes |
| Invest No Controller Ind | Yes |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Int Visual Exam Results | Localized Pitting |
| Int Water Acid Ind | Yes |
| Int Microbiological Ind | Yes |
| Int Metallurgical Basis Ind | Yes |
| Int Low Point Pipe Loc Ind | Yes |
| Corrosion Inhibitors | No |
| Corrosion Lining | No |
| Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
| Corrosion Coupons | Not Applicable - Not Mainline Pipe |
| Preparer Name | D******* S*** |
| Preparer Title | Hes Professional |
| Preparer Email | D*****@m****************.com |
| Preparer Telephone | 419-421-2121 |
| Prepared Date | 2015-10-06 00:00:00 |
| Authorizer Name | R****** W* B***** |
| Authorizer Telephone | 419-421-2121 |
| Authorizer Title | Regulatory And Compliance Supervisor |
| Authorizer Email | R*******@m****************.com |
| Narrative | During a routine station check, freestanding crude oil was discovered in two excavations associated with recent project work at the station. The source of the release was identified as internal corrosion on dead leg piping near the manifold. The piping was removed along with 9.24 tons of soil. |
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