HL incident on 2013-08-29 — OH

Operator
Marathon Pipe Line Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$92,500
Incident datetime
2013-08-29 07:34
Report number
Location
OH
Narrative
During a routine station check, freestanding crude oil was discovered in two excavations associated with recent project work at the station. The source of the release was identified as internal corrosion on dead leg piping near the manifold. The piping was removed along with 9.24 tons of soil.
Detailed record list
Report Received Date
2013-09-24 00:00:00
Iyear
2013
Report Number
20130328
Supplemental Number
20800
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2013-08-29 07:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
273
Recovered Bbls
273
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-08-29 07:34:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-08-29 07:34:00
Restart Datetime
2013-08-31 00:19:00
On Site Datetime
2013-08-29 07:34:00
Nrc Rpt Datetime
2013-08-29 08:42:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Martinsville Station
Segment Name
Patoka-Martinsville 20" And Martinsville-Lima 22"
Onshore State Abbreviation
Il
Onshore Postal Code
62442
Onshore City Name
Martinsville
Onshore County Name
Clark
Designated Location
Survey Station No.
Designated Name
Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Installation Year
2001
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
27095
Est Cost Prop Damage
92500
Est Cost Emergency
400000
Est Cost Environmental
0
Est Cost Other
0
Prpty
519595
Accident Psig
15
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
D******* S***
Preparer Title
Hes Professional
Preparer Email
D*****@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2015-10-06 00:00:00
Authorizer Name
R****** W* B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory And Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
During a routine station check, freestanding crude oil was discovered in two excavations associated with recent project work at the station. The source of the release was identified as internal corrosion on dead leg piping near the manifold. The piping was removed along with 9.24 tons of soil.
Report Received Date 2013-09-24 00:00:00
Iyear 2013
Report Number 20130328
Supplemental Number 20800
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2013-08-29 07:30:00
Location Latitude 39.3271159 Google Maps OpenStreetMap
Location Longitude -87.8981323 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 273
Recovered Bbls 273
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2013-08-29 07:34:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-08-29 07:34:00
Restart Datetime 2013-08-31 00:19:00
On Site Datetime 2013-08-29 07:34:00
Nrc Rpt Datetime 2013-08-29 08:42:00
Nrc Rpt Num 1058582 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Martinsville Station
Segment Name Patoka-Martinsville 20" And Martinsville-Lima 22"
Onshore State Abbreviation Il
Onshore Postal Code 62442
Onshore City Name Martinsville
Onshore County Name Clark
Designated Location Survey Station No.
Designated Name Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Relief Line And Relief Equipment
Installation Year 2001
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 27095
Est Cost Prop Damage 92500
Est Cost Emergency 400000
Est Cost Environmental 0
Est Cost Other 0
Prpty 519595
Accident Psig 15
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name D******* S***
Preparer Title Hes Professional
Preparer Email D*****@m****************.com
Preparer Telephone 419-421-2121
Prepared Date 2015-10-06 00:00:00
Authorizer Name R****** W* B*****
Authorizer Telephone 419-421-2121
Authorizer Title Regulatory And Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative During a routine station check, freestanding crude oil was discovered in two excavations associated with recent project work at the station. The source of the release was identified as internal corrosion on dead leg piping near the manifold. The piping was removed along with 9.24 tons of soil.

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