Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-08-29 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2013-08-29 08:00
Report number
Location
OK
Narrative
A flange on the extension to run the smart pig was not properly tightened.
Detailed record list
Report Received Date
2013-09-17 00:00:00
Iyear
2013
Report Number
20130316
Supplemental Number
18756
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2013-08-29 08:00:00
Location Latitude
32.39482
Location Longitude
-99.75808
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-08-29 08:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Flange Was Tightened While In-Service
On Site Datetime
2013-08-29 09:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Abilene Jct. Sta. No. 745
Segment Name
Line Id 6926 Midland To Corsicana 14/16"
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Abilene
Onshore County Name
Taylor
Designated Location
Milepost/valve Station
Designated Name
139.25
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
0
Est Cost Emergency
4500
Est Cost Environmental
0
Est Cost Other
0
Prpty
4650
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Preparer Name
D******* C*********
Preparer Title
Sr. Compliance Coordinator
Preparer Email
D******************@m*********.com
Preparer Telephone
9185747386
Prepared Date
2013-11-22 00:00:00
Authorizer Name
D******* C*********
Authorizer Telephone
9185747386
Authorizer Email
No Email Address
Narrative
A flange on the extension to run the smart pig was not properly tightened.
| Report Received Date | 2013-09-17 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130316 |
| Supplemental Number | 18756 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2013-08-29 08:00:00 |
| Location Latitude | 32.39482 Google Maps OpenStreetMap |
| Location Longitude | -99.75808 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 1 |
| Recovered Bbls | 1 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2013-08-29 08:00:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Flange Was Tightened While In-Service |
| On Site Datetime | 2013-08-29 09:00:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Abilene Jct. Sta. No. 745 |
| Segment Name | Line Id 6926 Midland To Corsicana 14/16" |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 79706 |
| Onshore City Name | Abilene |
| Onshore County Name | Taylor |
| Designated Location | Milepost/valve Station |
| Designated Name | 139.25 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Scraper/pig Trap |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 150 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 4500 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 4650 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage |
| Operation Type | Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage |
| Preparer Name | D******* C********* |
| Preparer Title | Sr. Compliance Coordinator |
| Preparer Email | D******************@m*********.com |
| Preparer Telephone | 9185747386 |
| Prepared Date | 2013-11-22 00:00:00 |
| Authorizer Name | D******* C********* |
| Authorizer Telephone | 9185747386 |
| Authorizer Email | No Email Address |
| Narrative | A flange on the extension to run the smart pig was not properly tightened. |
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