HL incident on 2013-08-21 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-08-21 16:25
Report number
Location
TX
Narrative
Routine maintenance (valve repair) was performed which required a 36" tank line and tank contents to be stripped empty to perform this task. Terminal operator blocked in the line stripping operation. The first operator had left the 2" bleeder valve opened. Whe the piping was used several days later, product flowed through the 2" bleeder valve, causing a blowdown tank to overfill and spill approximately 3 barrels of gas/oil mixture into containment and approximately 3 barrels into soil around the containment. The spill was reported by a contractor working in the area. Vacuum trucks were dispatched to remove the spilled product and pipeline operations were shut down until the spill was cleaned up.
Detailed record list
Report Received Date
2013-09-10 00:00:00
Iyear
2013
Report Number
20130310
Supplemental Number
18534
Report Type
Original Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-08-21 16:25:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
6
Recovered Bbls
6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-08-21 16:25:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-08-21 16:25:00
Restart Datetime
2013-08-21 20:00:00
On Site Datetime
2013-08-21 16:25:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Kinder Morgan
Segment Name
Colonial Manifold
Onshore State Abbreviation
Tx
Onshore Postal Code
77506
Onshore City Name
Pasadena
Onshore County Name
Harris
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Appurtenance
Tank Type
Atmospheric
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
500
Est Cost Environmental
1500
Est Cost Other
0
Prpty
2000
Accident Psig
14
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Invest Other Ind
Yes
Invest Other Ind Details
Procedure Was Not Followed By Field Operations Personnel. Ssp 6000 Dual Verification Procedure
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Other
Overflow Other Details
Blowdown Tank
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
D******* S*******
Preparer Title
Regulatory Compliance Manager
Preparer Telephone
713.725.0147
Prepared Date
2013-09-10 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
713.725.0147
Authorizer Title
Regulatory Compliance Manager
Narrative
Routine maintenance (valve repair) was performed which required a 36" tank line and tank contents to be stripped empty to perform this task. Terminal operator blocked in the line stripping operation. The first operator had left the 2" bleeder valve opened. Whe the piping was used several days later, product flowed through the 2" bleeder valve, causing a blowdown tank to overfill and spill approximately 3 barrels of gas/oil mixture into containment and approximately 3 barrels into soil around the containment. The spill was reported by a contractor working in the area. Vacuum trucks were dispatched to remove the spilled product and pipeline operations were shut down until the spill was cleaned up.
Report Received Date 2013-09-10 00:00:00
Iyear 2013
Report Number 20130310
Supplemental Number 18534
Report Type Original Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-08-21 16:25:00
Location Latitude 29.73064 Google Maps OpenStreetMap
Location Longitude -95.20349 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 6
Recovered Bbls 6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2013-08-21 16:25:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-08-21 16:25:00
Restart Datetime 2013-08-21 20:00:00
On Site Datetime 2013-08-21 16:25:00
Ignite Ind No
Explode Ind No
Pipe Fac Name Kinder Morgan
Segment Name Colonial Manifold
Onshore State Abbreviation Tx
Onshore Postal Code 77506
Onshore City Name Pasadena
Onshore County Name Harris
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Appurtenance
Tank Type Atmospheric
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 500
Est Cost Environmental 1500
Est Cost Other 0
Prpty 2000
Accident Psig 14
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Invest Other Ind Yes
Invest Other Ind Details Procedure Was Not Followed By Field Operations Personnel. Ssp 6000 Dual Verification Procedure
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Other
Overflow Other Details Blowdown Tank
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name D******* S*******
Preparer Title Regulatory Compliance Manager
Preparer Telephone 713.725.0147
Prepared Date 2013-09-10 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 713.725.0147
Authorizer Title Regulatory Compliance Manager
Narrative Routine maintenance (valve repair) was performed which required a 36" tank line and tank contents to be stripped empty to perform this task. Terminal operator blocked in the line stripping operation. The first operator had left the 2" bleeder valve opened. Whe the piping was used several days later, product flowed through the 2" bleeder valve, causing a blowdown tank to overfill and spill approximately 3 barrels of gas/oil mixture into containment and approximately 3 barrels into soil around the containment. The spill was reported by a contractor working in the area. Vacuum trucks were dispatched to remove the spilled product and pipeline operations were shut down until the spill was cleaned up.

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