HL incident on 2013-07-18 — TX

Operator
Chevron Petrochemical Pipeline Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$322,200
Incident datetime
2013-07-18 16:15
Report number
Location
TX
Narrative
The analytical report confirms that the root cause of the leak was a manufacturing defect of x52 erw pipe. The size of the anomaly would not be considered a defect per ap 5lx standards in 1953, or the current API 5lx edition. Therefore, there are no previous or current nde methods including ili tools that would be able to detect this type of anomaly. The root cause in the analytical report reads as follows: 1. The erw seam leak was caused by a cold weld, a typical manufacture defect in low-frequency erw seams. This conclusion was supported by the following characteris including the smooth fracture surfaces at the leak, the through-wall oxide layer, and no evidence of bonding. 2. The most likely cause of the cold weld was insufficient heat and/or forming tool pressure during manufacture. 3. The pipe dimension and mechanical properties met the requirement specified in API standard 5lx fourth edition (1953) for grade x52 line pipe. The base metal microstructure was ferrite plus pearlite, as is typical of carbon manganese steel pipe.
Detailed record list
Report Received Date
2013-09-09 00:00:00
Iyear
2013
Report Number
20130305
Supplemental Number
19139
Report Type
Supplemental Final
Operator Id
Name
Chevron Petrochemical Pipeline Llc
Operator Street Address
9 Greenway Plaza
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046
Local Datetime
2013-07-18 16:15:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethylene
Unintentional Release Bbls
0
Intentional Release Bbls
17825
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-07-18 16:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-08-01 14:00:00
Restart Datetime
2014-02-20 05:00:00
On Site Datetime
2013-07-18 16:15:00
Nrc Rpt Datetime
2013-08-28 16:28:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Evangeline Ethylene Pipeline System
Segment Name
Sabine River East Mlv To Gum Cove Mlv
Onshore State Abbreviation
La
Onshore Postal Code
70663
Onshore City Name
Sulphur
Onshore County Name
Calcasieu
Designated Location
Milepost/valve Station
Designated Name
26.7
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
16
Pipe Wall Thickness
0.312
Pipe Smys
52000
Pipe Specification
Api 5lx
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Youngstown Steel And Tube Company, Ny
Pipe Coating Type
Coal Tar
Installation Year
1954
Manufactured Year
1953
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
995728
Est Cost Prop Damage
322200
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1317928
Accident Psig
1100
Mop Psig
1175
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Not Mandated
Length Segment Isolated
71273
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pinhole leak volume was so small that it could not be detected by scada
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Erw Longitudinal Seam Cold Weld
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2012
Geometry Recent Year
2012
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2001
Hydrtst Most Rcnt Pressure
1681
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
H**** L* L****
Preparer Title
Dot Pipeline Safety Specialist
Preparer Email
H*********@c******.com
Preparer Telephone
3376548915
Preparer Fax
3375723720
Prepared Date
2014-03-18 00:00:00
Authorizer Name
H**** L* L****
Authorizer Telephone
3376548915
Authorizer Title
Dot Pipeline Safety Specialist
Authorizer Email
H*********@c******.com
Narrative
The analytical report confirms that the root cause of the leak was a manufacturing defect of x52 erw pipe. The size of the anomaly would not be considered a defect per ap 5lx standards in 1953, or the current API 5lx edition. Therefore, there are no previous or current nde methods including ili tools that would be able to detect this type of anomaly. The root cause in the analytical report reads as follows: 1. The erw seam leak was caused by a cold weld, a typical manufacture defect in low-frequency erw seams. This conclusion was supported by the following characteris including the smooth fracture surfaces at the leak, the through-wall oxide layer, and no evidence of bonding. 2. The most likely cause of the cold weld was insufficient heat and/or forming tool pressure during manufacture. 3. The pipe dimension and mechanical properties met the requirement specified in API standard 5lx fourth edition (1953) for grade x52 line pipe. The base metal microstructure was ferrite plus pearlite, as is typical of carbon manganese steel pipe.
Report Received Date 2013-09-09 00:00:00
Iyear 2013
Report Number 20130305
Supplemental Number 19139
Report Type Supplemental Final
Operator Id 31554 PHMSA Enforcement
Name Chevron Petrochemical Pipeline Llc
Operator Street Address 9 Greenway Plaza
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046
Local Datetime 2013-07-18 16:15:00
Location Latitude 30.060572 Google Maps OpenStreetMap
Location Longitude -93.5581 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethylene
Unintentional Release Bbls 0
Intentional Release Bbls 17825
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2013-07-18 16:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-08-01 14:00:00
Restart Datetime 2014-02-20 05:00:00
On Site Datetime 2013-07-18 16:15:00
Nrc Rpt Datetime 2013-08-28 16:28:00
Nrc Rpt Num 1058513 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Evangeline Ethylene Pipeline System
Segment Name Sabine River East Mlv To Gum Cove Mlv
Onshore State Abbreviation La
Onshore Postal Code 70663
Onshore City Name Sulphur
Onshore County Name Calcasieu
Designated Location Milepost/valve Station
Designated Name 26.7
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 16
Pipe Wall Thickness 0.312
Pipe Smys 52000
Pipe Specification Api 5lx
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Youngstown Steel And Tube Company, Ny
Pipe Coating Type Coal Tar
Installation Year 1954
Manufactured Year 1953
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 995728
Est Cost Prop Damage 322200
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1317928
Accident Psig 1100
Mop Psig 1175
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Not Mandated
Length Segment Isolated 71273
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pinhole leak volume was so small that it could not be detected by scada
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Erw Longitudinal Seam Cold Weld
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2012
Geometry Recent Year 2012
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2001
Hydrtst Most Rcnt Pressure 1681
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name H**** L* L****
Preparer Title Dot Pipeline Safety Specialist
Preparer Email H*********@c******.com
Preparer Telephone 3376548915
Preparer Fax 3375723720
Prepared Date 2014-03-18 00:00:00
Authorizer Name H**** L* L****
Authorizer Telephone 3376548915
Authorizer Title Dot Pipeline Safety Specialist
Authorizer Email H*********@c******.com
Narrative The analytical report confirms that the root cause of the leak was a manufacturing defect of x52 erw pipe. The size of the anomaly would not be considered a defect per ap 5lx standards in 1953, or the current API 5lx edition. Therefore, there are no previous or current nde methods including ili tools that would be able to detect this type of anomaly. The root cause in the analytical report reads as follows: 1. The erw seam leak was caused by a cold weld, a typical manufacture defect in low-frequency erw seams. This conclusion was supported by the following characteris including the smooth fracture surfaces at the leak, the through-wall oxide layer, and no evidence of bonding. 2. The most likely cause of the cold weld was insufficient heat and/or forming tool pressure during manufacture. 3. The pipe dimension and mechanical properties met the requirement specified in API standard 5lx fourth edition (1953) for grade x52 line pipe. The base metal microstructure was ferrite plus pearlite, as is typical of carbon manganese steel pipe.

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