HL incident on 2013-08-13 — PA

Operator
Buckeye Partners, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-08-13 14:55
Report number
Location
PA
Narrative
At 14:55 on august 13, 2013 during the return to service operat tank 91 walk around, a buckeye operator noticed transmix spraying out of a 1/2" opened valve that is located directly behind a 6" valve. Tank filling operations were immediately stopped. All internal and external notifications were made according to company procedures and policies. Investigations revealed that the bung was not properly closed on the 1/2 valve. The valve bung was closed and filling operations resumed. All contaminated product was removed. No additional remediation is required
Detailed record list
Report Received Date
2013-09-06 00:00:00
Iyear
2013
Report Number
20130301
Supplemental Number
18514
Report Type
Original Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2013-08-13 14:55:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
1.85
Recovered Bbls
1.83
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-08-13 14:55:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Operations To Fill The Tank Were Halted.
On Site Datetime
2013-08-13 14:55:00
Nrc Rpt Datetime
2013-08-13 16:25:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Linden Station
Segment Name
Ln
Onshore State Abbreviation
Nj
Onshore Postal Code
07036
Onshore City Name
Linden
Onshore County Name
Union
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Release Type
Leak
Leak Type
Other
Leak Type Other
1/2" Drain
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
2000
Est Cost Environmental
25000
Est Cost Other
0
Prpty
27000
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name
H*** S******
Preparer Title
Sr. Compliance Specialist
Preparer Email
H*******@b******.com
Preparer Telephone
610-904-4916
Prepared Date
2013-09-06 00:00:00
Authorizer Name
J*** R*******
Authorizer Telephone
610-904-4185
Authorizer Title
Compliance Manager
Authorizer Email
J********@b******.com
Narrative
At 14:55 on august 13, 2013 during the return to service operat tank 91 walk around, a buckeye operator noticed transmix spraying out of a 1/2" opened valve that is located directly behind a 6" valve. Tank filling operations were immediately stopped. All internal and external notifications were made according to company procedures and policies. Investigations revealed that the bung was not properly closed on the 1/2 valve. The valve bung was closed and filling operations resumed. All contaminated product was removed. No additional remediation is required
Report Received Date 2013-09-06 00:00:00
Iyear 2013
Report Number 20130301
Supplemental Number 18514
Report Type Original Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2013-08-13 14:55:00
Location Latitude 40.605222 Google Maps OpenStreetMap
Location Longitude -74.23907 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 1.85
Recovered Bbls 1.83
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2013-08-13 14:55:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Operations To Fill The Tank Were Halted.
On Site Datetime 2013-08-13 14:55:00
Nrc Rpt Datetime 2013-08-13 16:25:00
Nrc Rpt Num 1057004 NRC Report How to search
Ignite Ind No
Explode Ind No
Pipe Fac Name Linden Station
Segment Name Ln
Onshore State Abbreviation Nj
Onshore Postal Code 07036
Onshore City Name Linden
Onshore County Name Union
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Pipe Facility Type Interstate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Release Type Leak
Leak Type Other
Leak Type Other 1/2" Drain
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 2000
Est Cost Environmental 25000
Est Cost Other 0
Prpty 27000
Pipeline Function < 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Preparer Name H*** S******
Preparer Title Sr. Compliance Specialist
Preparer Email H*******@b******.com
Preparer Telephone 610-904-4916
Prepared Date 2013-09-06 00:00:00
Authorizer Name J*** R*******
Authorizer Telephone 610-904-4185
Authorizer Title Compliance Manager
Authorizer Email J********@b******.com
Narrative At 14:55 on august 13, 2013 during the return to service operat tank 91 walk around, a buckeye operator noticed transmix spraying out of a 1/2" opened valve that is located directly behind a 6" valve. Tank filling operations were immediately stopped. All internal and external notifications were made according to company procedures and policies. Investigations revealed that the bung was not properly closed on the 1/2 valve. The valve bung was closed and filling operations resumed. All contaminated product was removed. No additional remediation is required

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