HL incident on 2013-08-03 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$180,220
Incident datetime
2013-08-03 09:18
Report number
Location
TX
Narrative
At approximately 9:10 a.M. On august 3, edmonton control center (ecc) observed zero flow on meter 3 at the griffith terminal during delivery to bp. The ecc contacted the gauger on duty to investigate. At 9:18 a.M. Gauger confirmed leak at meter skid. At approximately 9:20 a.M., gauger contacted the ecc to shut down the delivery line and placed call to terminal supervisor and left a message. Gauger then contacted pipeline maintenance supervisor to notify him of the release. Gauger then took the necessary steps to secure release site and stop all work in the terminal. All workers on site were evacuated to the east gate. Pipeline maintenance crews were notified and onsite at approximately 9:25 a.M. Gauger identified meter 3 as the leak source at approximately 9:30 a.M. Terminal supervisor returned call to gauger at 9:45 a.M. And was informed of the release. At approximately 9:50 a.M. Terminal supervisor notified area manager on call. Area manager then notified environment who in turn notified the state of indiana. At 10:51 a.M. Area manager placed call to the national response center. It was determined that the release of oil was from a meter housing failure on 155-meter 3 due to the failure of two cap screws in the housing. The meter was removed from service and isolated. Root cause of meter housing failure is under investigation. A supplemental report will be done once the investigation is completed. Approximately 306.6 tons of contaminated soil was disposed of at an approved site.
Detailed record list
Report Received Date
2013-08-30 00:00:00
Iyear
2013
Report Number
20130295
Supplemental Number
19343
Report Type
Supplemental Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2013-08-03 09:18:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
160
Recovered Bbls
160
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-08-03 09:18:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-08-03 09:24:00
Restart Datetime
2013-08-04 00:24:00
On Site Datetime
2013-08-03 09:25:00
Nrc Rpt Datetime
2013-08-03 10:51:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Griffith Terminal
Segment Name
Meter Skid 155 Meter 3
Onshore State Abbreviation
In
Onshore Postal Code
46319
Onshore City Name
Griffith
Onshore County Name
Lake
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Meter Housing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
180220
Est Cost Emergency
175000
Est Cost Environmental
481049
Est Cost Other
0
Prpty
836469
Accident Psig
182
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Invest Other Ind
Yes
Invest Other Ind Details
Investigation Identified Equipment Failure On Meter Manifold
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
1" Cinch Bolts On Meter Housing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Upward, Axial, Force On Meter Inner Mechanism
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
218-464-5754
Preparer Fax
218-464-5992
Prepared Date
2014-05-01 00:00:00
Authorizer Name
D**** S*******
Authorizer Telephone
218-464-5751
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
D*************@e*******.com
Narrative
At approximately 9:10 a.M. On august 3, edmonton control center (ecc) observed zero flow on meter 3 at the griffith terminal during delivery to bp. The ecc contacted the gauger on duty to investigate. At 9:18 a.M. Gauger confirmed leak at meter skid. At approximately 9:20 a.M., gauger contacted the ecc to shut down the delivery line and placed call to terminal supervisor and left a message. Gauger then contacted pipeline maintenance supervisor to notify him of the release. Gauger then took the necessary steps to secure release site and stop all work in the terminal. All workers on site were evacuated to the east gate. Pipeline maintenance crews were notified and onsite at approximately 9:25 a.M. Gauger identified meter 3 as the leak source at approximately 9:30 a.M. Terminal supervisor returned call to gauger at 9:45 a.M. And was informed of the release. At approximately 9:50 a.M. Terminal supervisor notified area manager on call. Area manager then notified environment who in turn notified the state of indiana. At 10:51 a.M. Area manager placed call to the national response center. It was determined that the release of oil was from a meter housing failure on 155-meter 3 due to the failure of two cap screws in the housing. The meter was removed from service and isolated. Root cause of meter housing failure is under investigation. A supplemental report will be done once the investigation is completed. Approximately 306.6 tons of contaminated soil was disposed of at an approved site.
Report Received Date 2013-08-30 00:00:00
Iyear 2013
Report Number 20130295
Supplemental Number 19343
Report Type Supplemental Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2013-08-03 09:18:00
Location Latitude 41.51616 Google Maps OpenStreetMap
Location Longitude -87.44906 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 160
Recovered Bbls 160
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2013-08-03 09:18:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-08-03 09:24:00
Restart Datetime 2013-08-04 00:24:00
On Site Datetime 2013-08-03 09:25:00
Nrc Rpt Datetime 2013-08-03 10:51:00
Nrc Rpt Num 1055996 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Griffith Terminal
Segment Name Meter Skid 155 Meter 3
Onshore State Abbreviation In
Onshore Postal Code 46319
Onshore City Name Griffith
Onshore County Name Lake
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Meter/prover
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Meter Housing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 180220
Est Cost Emergency 175000
Est Cost Environmental 481049
Est Cost Other 0
Prpty 836469
Accident Psig 182
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Invest Other Ind Yes
Invest Other Ind Details Investigation Identified Equipment Failure On Meter Manifold
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details 1" Cinch Bolts On Meter Housing
Eq Additional Other Ind Yes
Eq Additional Other Details Upward, Axial, Force On Meter Inner Mechanism
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 218-464-5754
Preparer Fax 218-464-5992
Prepared Date 2014-05-01 00:00:00
Authorizer Name D**** S*******
Authorizer Telephone 218-464-5751
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email D*************@e*******.com
Narrative At approximately 9:10 a.M. On august 3, edmonton control center (ecc) observed zero flow on meter 3 at the griffith terminal during delivery to bp. The ecc contacted the gauger on duty to investigate. At 9:18 a.M. Gauger confirmed leak at meter skid. At approximately 9:20 a.M., gauger contacted the ecc to shut down the delivery line and placed call to terminal supervisor and left a message. Gauger then contacted pipeline maintenance supervisor to notify him of the release. Gauger then took the necessary steps to secure release site and stop all work in the terminal. All workers on site were evacuated to the east gate. Pipeline maintenance crews were notified and onsite at approximately 9:25 a.M. Gauger identified meter 3 as the leak source at approximately 9:30 a.M. Terminal supervisor returned call to gauger at 9:45 a.M. And was informed of the release. At approximately 9:50 a.M. Terminal supervisor notified area manager on call. Area manager then notified environment who in turn notified the state of indiana. At 10:51 a.M. Area manager placed call to the national response center. It was determined that the release of oil was from a meter housing failure on 155-meter 3 due to the failure of two cap screws in the housing. The meter was removed from service and isolated. Root cause of meter housing failure is under investigation. A supplemental report will be done once the investigation is completed. Approximately 306.6 tons of contaminated soil was disposed of at an approved site.

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