HL incident on 2013-08-01 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$42,700
Incident datetime
2013-08-01 09:40
Report number
Location
TX
Narrative
On 8/1/2013, an aerial patrol pilot informed the jackson station technician of dead vegetation near am 428. The technician drove to the site and discovered a 15' radius of stunted growth of corn above enterprise's west leg blue line. The technician found elevated lel at ground level in the cracks of the ground. The line was not running at the time. The technician informed pipeline control who lowered pressure on the line. The leaking segment was then blocked in between am 422 and am 432. The area was excavated and a small bubble leak was found at the thread of the bleeder valve on the stopple blind flange. The leak stopped and lel readings were not detected once the bleeder valve was tightened. To mitigate future leak potential due to failure at the thread, a tor was welded on the blind flange to encase the bleeder valve. The pipeline was restarted on 8/9/2013 at 10:00 am.
Detailed record list
Report Received Date
2013-08-30 00:00:00
Iyear
2013
Report Number
20130294
Supplemental Number
18987
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-08-01 09:40:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
0.2
Intentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-08-01 09:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Already Shut Down At The Time.
On Site Datetime
2013-08-01 09:40:00
Nrc Rpt Datetime
2013-08-01 11:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
West Leg Blue Line
Segment Name
Lid 410
Onshore State Abbreviation
Mn
Onshore Postal Code
56176
Onshore City Name
Trimont
Onshore County Name
Martin
Designated Location
Milepost/valve Station
Designated Name
Am 428
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Pipe Facility Type
Interstate
Item Involved
Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
1200
Est Cost Gas Released
0
Est Cost Prop Damage
42700
Est Cost Emergency
2400
Est Cost Environmental
0
Est Cost Other
0
Prpty
46300
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Preparer Name
N*** T*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
N*******@e****.com
Preparer Telephone
713-381-2493
Prepared Date
2014-02-05 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
N*******@e****.com
Narrative
On 8/1/2013, an aerial patrol pilot informed the jackson station technician of dead vegetation near am 428. The technician drove to the site and discovered a 15' radius of stunted growth of corn above enterprise's west leg blue line. The technician found elevated lel at ground level in the cracks of the ground. The line was not running at the time. The technician informed pipeline control who lowered pressure on the line. The leaking segment was then blocked in between am 422 and am 432. The area was excavated and a small bubble leak was found at the thread of the bleeder valve on the stopple blind flange. The leak stopped and lel readings were not detected once the bleeder valve was tightened. To mitigate future leak potential due to failure at the thread, a tor was welded on the blind flange to encase the bleeder valve. The pipeline was restarted on 8/9/2013 at 10:00 am.
Report Received Date 2013-08-30 00:00:00
Iyear 2013
Report Number 20130294
Supplemental Number 18987
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-08-01 09:40:00
Location Latitude 43.78507 Google Maps OpenStreetMap
Location Longitude -94.624817 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 0.2
Intentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2013-08-01 09:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline Was Already Shut Down At The Time.
On Site Datetime 2013-08-01 09:40:00
Nrc Rpt Datetime 2013-08-01 11:15:00
Nrc Rpt Num 1055769 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name West Leg Blue Line
Segment Name Lid 410
Onshore State Abbreviation Mn
Onshore Postal Code 56176
Onshore City Name Trimont
Onshore County Name Martin
Designated Location Milepost/valve Station
Designated Name Am 428
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Pipe Facility Type Interstate
Item Involved Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Release Type Leak
Leak Type Connection Failure
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 1200
Est Cost Gas Released 0
Est Cost Prop Damage 42700
Est Cost Emergency 2400
Est Cost Environmental 0
Est Cost Other 0
Prpty 46300
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Preparer Name N*** T*****
Preparer Title Pipeline Compliance Engineer
Preparer Email N*******@e****.com
Preparer Telephone 713-381-2493
Prepared Date 2014-02-05 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 713-381-2493
Authorizer Title Pipeline Compliance Engineer
Authorizer Email N*******@e****.com
Narrative On 8/1/2013, an aerial patrol pilot informed the jackson station technician of dead vegetation near am 428. The technician drove to the site and discovered a 15' radius of stunted growth of corn above enterprise's west leg blue line. The technician found elevated lel at ground level in the cracks of the ground. The line was not running at the time. The technician informed pipeline control who lowered pressure on the line. The leaking segment was then blocked in between am 422 and am 432. The area was excavated and a small bubble leak was found at the thread of the bleeder valve on the stopple blind flange. The leak stopped and lel readings were not detected once the bleeder valve was tightened. To mitigate future leak potential due to failure at the thread, a tor was welded on the blind flange to encase the bleeder valve. The pipeline was restarted on 8/9/2013 at 10:00 am.

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