HL incident on 2013-07-22 — TX

Operator
The Dow Chemical Company
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$30,000
Incident datetime
2013-07-22 15:30
Report number
Location
TX
Narrative
On july 22, 2013, the dow chemical company officially reported a leak on a pygas pipeline, dpl-191. The national response center report number for this incident is 1054720 and the railroad commission of texas incident number is 825. Low pressure hydrotesting the line confirmed that the pipeline had a pinhole leak in a girth weld. Metallurgical analysis from cut-outs taken of the line indicated that brine water constituents from the pygas storage well were a probable cause of the internal corrosion in the locally affected zone closest to the storage well (area where pinhole leak was found). Once the leak was discovered, the line was shut down, cleaned and cleared. Currently, dow is assessing the pipeline for any further corrosion or issues. The surrounding area has been properly remediated and all product has been recovered. On 1/19/2015 - updated the smys. Was incorrectly entered as %smys.
Detailed record list
Report Received Date
2013-08-22 00:00:00
Iyear
2013
Report Number
20130284
Supplemental Number
20064
Report Type
Supplemental
Operator Id
Name
The Dow Chemical Company
Operator Street Address
6723 E. Hwy 332 Bldg Bm-59
Operator City Name
Freeport
Operator State Abbreviation
TX
Operator Postal Code
77541
Local Datetime
2013-07-22 15:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Pygas
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-07-22 15:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-07-22 15:45:00
Still Shutdown Ind
Yes
On Site Datetime
2013-07-22 15:45:00
Nrc Rpt Datetime
2013-07-22 16:46:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
The Dow Chemical Company
Segment Name
Dpl-191
Onshore State Abbreviation
Tx
Onshore Postal Code
77531
Onshore City Name
Clute
Onshore County Name
Brazoria
Designated Location
Survey Station No.
Designated Name
Ww-282
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
29
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
10
Pipe Wall Thickness
0.218
Pipe Smys
60000
Pipe Specification
Api 5lx60
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
U.s. Steel
Pipe Coating Type
Extruded Polyehylene
Weld Subtype
Pipe Girth Weld
Installation Year
1977
Manufactured Year
1977
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1000
Est Cost Prop Damage
30000
Est Cost Emergency
5000
Est Cost Environmental
200000
Est Cost Other
0
Prpty
236000
Accident Psig
250
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
26244
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was not deemed due to operator error or input. Line had been idle for a period of time and was being brought out of idle and into full service. No pressure spikes or surges.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Corrosive Commodity Ind
Yes
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Girth Weld
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
No
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2013
Other Recent Year
2013
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2013
Hydrtst Most Rcnt Pressure
1642
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S****** N*********
Preparer Title
Compliance Leader
Preparer Email
S***********@d**.com
Preparer Telephone
979-238-5964
Preparer Fax
979-238-0911
Prepared Date
2015-01-19 00:00:00
Authorizer Name
R*** T*****
Authorizer Telephone
979-238-4770
Authorizer Title
Process Leader
Authorizer Email
T*******@d**.com
Narrative
On july 22, 2013, the dow chemical company officially reported a leak on a pygas pipeline, dpl-191. The national response center report number for this incident is 1054720 and the railroad commission of texas incident number is 825. Low pressure hydrotesting the line confirmed that the pipeline had a pinhole leak in a girth weld. Metallurgical analysis from cut-outs taken of the line indicated that brine water constituents from the pygas storage well were a probable cause of the internal corrosion in the locally affected zone closest to the storage well (area where pinhole leak was found). Once the leak was discovered, the line was shut down, cleaned and cleared. Currently, dow is assessing the pipeline for any further corrosion or issues. The surrounding area has been properly remediated and all product has been recovered. On 1/19/2015 - updated the smys. Was incorrectly entered as %smys.
Report Received Date 2013-08-22 00:00:00
Iyear 2013
Report Number 20130284
Supplemental Number 20064
Report Type Supplemental
Operator Id 30959 PHMSA Enforcement
Name The Dow Chemical Company
Operator Street Address 6723 E. Hwy 332 Bldg Bm-59
Operator City Name Freeport
Operator State Abbreviation TX
Operator Postal Code 77541
Local Datetime 2013-07-22 15:30:00
Location Latitude 29.04718 Google Maps OpenStreetMap
Location Longitude -95.35215 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Pygas
Unintentional Release Bbls 0.2
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2013-07-22 15:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-07-22 15:45:00
Still Shutdown Ind Yes
On Site Datetime 2013-07-22 15:45:00
Nrc Rpt Datetime 2013-07-22 16:46:00
Nrc Rpt Num 1054720 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name The Dow Chemical Company
Segment Name Dpl-191
Onshore State Abbreviation Tx
Onshore Postal Code 77531
Onshore City Name Clute
Onshore County Name Brazoria
Designated Location Survey Station No.
Designated Name Ww-282
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 29
Crossing No
Pipe Facility Type Intrastate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 10
Pipe Wall Thickness 0.218
Pipe Smys 60000
Pipe Specification Api 5lx60
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer U.s. Steel
Pipe Coating Type Extruded Polyehylene
Weld Subtype Pipe Girth Weld
Installation Year 1977
Manufactured Year 1977
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1000
Est Cost Prop Damage 30000
Est Cost Emergency 5000
Est Cost Environmental 200000
Est Cost Other 0
Prpty 236000
Accident Psig 250
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 26244
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was not deemed due to operator error or input. Line had been idle for a period of time and was being brought out of idle and into full service. No pressure spikes or surges.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Corrosive Commodity Ind Yes
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Metallurgical Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Girth Weld
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons No
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2013
Other Recent Year 2013
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2013
Hydrtst Most Rcnt Pressure 1642
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S****** N*********
Preparer Title Compliance Leader
Preparer Email S***********@d**.com
Preparer Telephone 979-238-5964
Preparer Fax 979-238-0911
Prepared Date 2015-01-19 00:00:00
Authorizer Name R*** T*****
Authorizer Telephone 979-238-4770
Authorizer Title Process Leader
Authorizer Email T*******@d**.com
Narrative On july 22, 2013, the dow chemical company officially reported a leak on a pygas pipeline, dpl-191. The national response center report number for this incident is 1054720 and the railroad commission of texas incident number is 825. Low pressure hydrotesting the line confirmed that the pipeline had a pinhole leak in a girth weld. Metallurgical analysis from cut-outs taken of the line indicated that brine water constituents from the pygas storage well were a probable cause of the internal corrosion in the locally affected zone closest to the storage well (area where pinhole leak was found). Once the leak was discovered, the line was shut down, cleaned and cleared. Currently, dow is assessing the pipeline for any further corrosion or issues. The surrounding area has been properly remediated and all product has been recovered. On 1/19/2015 - updated the smys. Was incorrectly entered as %smys.

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