HL incident on 2013-07-22 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,446
Incident datetime
2013-07-22 07:18
Report number
Location
TX
Narrative
At approximately 6:58 am, the deer river technician arrived at the station and noticed a crude oil smell. He looked around and found oil around the line 4 sending trap door, and immediately contacted the area manager at 7:18 am. The trap was isolated until the cause of the leak was determined and the repair could be completed. The bemidji plm arrived at deer river station around 9:30 am to investigate further and found that the o ring on the trap door was defective which caused the release of approx. 3.3 barrels. A new o ring was fabricated on site and replaced that same day. The defective o ring has been sent to a third party for analysis. Approximately 60 yards of contaminated soil was disposed of at an approved site.
Detailed record list
Report Received Date
2013-08-20 00:00:00
Iyear
2013
Report Number
20130280
Supplemental Number
18459
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2013-07-22 06:58:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3.33
Recovered Bbls
3.33
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-07-22 07:18:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Station Is Isolated And Bypassed
On Site Datetime
2013-07-22 07:18:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Line 4/dr
Segment Name
Line 4 Sending Trap Door
Onshore State Abbreviation
Mn
Onshore Postal Code
56636
Onshore City Name
Deer River
Onshore County Name
Itasca
Designated Location
Milepost/valve Station
Designated Name
995.91
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
2446
Est Cost Emergency
22010
Est Cost Environmental
11000
Est Cost Other
0
Prpty
35456
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
218-464-5754
Preparer Fax
218-464-5992
Prepared Date
2013-08-20 00:00:00
Authorizer Name
D**** S*******
Authorizer Telephone
218-464-5751
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
D*************@e*******.com
Narrative
At approximately 6:58 am, the deer river technician arrived at the station and noticed a crude oil smell. He looked around and found oil around the line 4 sending trap door, and immediately contacted the area manager at 7:18 am. The trap was isolated until the cause of the leak was determined and the repair could be completed. The bemidji plm arrived at deer river station around 9:30 am to investigate further and found that the o ring on the trap door was defective which caused the release of approx. 3.3 barrels. A new o ring was fabricated on site and replaced that same day. The defective o ring has been sent to a third party for analysis. Approximately 60 yards of contaminated soil was disposed of at an approved site.
Report Received Date 2013-08-20 00:00:00
Iyear 2013
Report Number 20130280
Supplemental Number 18459
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2013-07-22 06:58:00
Location Latitude 47.32444 Google Maps OpenStreetMap
Location Longitude -93.76306 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3.33
Recovered Bbls 3.33
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2013-07-22 07:18:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Station Is Isolated And Bypassed
On Site Datetime 2013-07-22 07:18:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Line 4/dr
Segment Name Line 4 Sending Trap Door
Onshore State Abbreviation Mn
Onshore Postal Code 56636
Onshore City Name Deer River
Onshore County Name Itasca
Designated Location Milepost/valve Station
Designated Name 995.91
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 2446
Est Cost Emergency 22010
Est Cost Environmental 11000
Est Cost Other 0
Prpty 35456
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 218-464-5754
Preparer Fax 218-464-5992
Prepared Date 2013-08-20 00:00:00
Authorizer Name D**** S*******
Authorizer Telephone 218-464-5751
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email D*************@e*******.com
Narrative At approximately 6:58 am, the deer river technician arrived at the station and noticed a crude oil smell. He looked around and found oil around the line 4 sending trap door, and immediately contacted the area manager at 7:18 am. The trap was isolated until the cause of the leak was determined and the repair could be completed. The bemidji plm arrived at deer river station around 9:30 am to investigate further and found that the o ring on the trap door was defective which caused the release of approx. 3.3 barrels. A new o ring was fabricated on site and replaced that same day. The defective o ring has been sent to a third party for analysis. Approximately 60 yards of contaminated soil was disposed of at an approved site.

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