HL incident on 2013-07-09 — MT

Operator
Cenex Pipeline Llc
Cause
Notification Issue
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$30,000
Incident datetime
2013-07-09 15:02
Report number
Location
MT
Narrative
On july 9, 2013, cenex pipeline was delivering product into the glendive terminal with the balance pumping to minot, nd at a rate of approximately 1100 barrels per hour. At approximately 3:02 p.M. Mdt, the cenex pipeline controller noticed a significant pressure drop at the discharge of glendive terminal and arnegard station. The controller began to shut down the 8 inch diameter pipeline segment between glendive and minot as a result of an unexplained pressure drop and had the pipeline shutdown and rov's closed by 3:05 and 25 seconds. At approximately 3:11 p.M., a representative of the excavator phoned the control center to report that their company may have hit the pipeline during excavation and believe that it is damaged. The excavator reported the approximate location of the release in the area between alexander and arnegard in section 26 and 27. The puncture occurred near cenex pipeline mile post 81, and a photograph of the damaged pipe is included in exhibit section 7. Cenex pipeline estimates that 870 barrels of gasoline was released at the site with approximately 38 barrels of free product being recovered. The released product did not ignite, did not reach any surface water, and there were no reported injuries or fatalities as a result of this release. The cause of this damage was determined to be excavator failure to notify the one call center of a change in location of the excavation. The excavator rerouted the excavation 373' away from the original planned excavation route, that was previously marked by cenex pipeline and hydro excavated at the planned crossing location, in coordination with the excavator. The reroute location was within view of the existing cenex pipeline markings at the planned excavation location. Upon deciding to reroute the excavation, the excavator failed to contact nd one call to request a new locate nor did they contact cenex pipeline to provide notification of the change in route. 1353 tons of contaminated soil were transported to ihd solids management, llc - williston, nd for disposal.
Detailed record list
Report Received Date
2013-08-07 00:00:00
Iyear
2013
Report Number
20130269
Supplemental Number
18656
Report Type
Supplemental Final
Operator Id
Name
Cenex Pipeline Llc
Operator Street Address
803 Hwy 212 S (Po Box 909)
Operator City Name
Laurel
Operator State Abbreviation
MT
Operator Postal Code
59044
Local Datetime
2013-07-09 15:02:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
870
Recovered Bbls
820
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2013-07-09 15:02:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-07-09 15:05:00
Restart Datetime
2013-07-12 17:45:00
On Site Datetime
2013-07-09 17:15:00
Nrc Rpt Datetime
2013-07-09 15:28:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Glendive To Minot 8"
Segment Name
Glendive To Minot 8"
Onshore State Abbreviation
Nd
Onshore Postal Code
58835
Onshore City Name
Nearest City Was Arnegard, Nd
Onshore County Name
Mckenzie
Designated Location
Milepost/valve Station
Designated Name
81
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.188
Pipe Smys
46000
Pipe Specification
Api 5l X46
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Cal-Metal
Pipe Coating Type
Coal Tar
Installation Year
1960
Manufactured Year
1960
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
7
Puncture Circum
9
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
15000
Est Cost Gas Released
110000
Est Cost Prop Damage
30000
Est Cost Emergency
150000
Est Cost Environmental
220000
Est Cost Other
50000
Est Cost Other Details
Continued Monitoring.
Prpty
575000
Accident Psig
500
Mop Psig
1135
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
453244
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind
Yes
Invest No Schedule Ind Details
It Was Determined That Controller Action Did Not Contribute To This Incident. The Controller Followed Procedures And Responded Appropriately And Promptly To The Incident, Therefore There Was No Cause To Further Investigate Fatigue.
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Water
One Call Notified Ind
Yes
One Call Ticket Num
13093161
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
75
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
M******* S*****
Preparer Title
Dot Compliance Coordinator
Preparer Email
M**************@c*****.com
Preparer Telephone
406-628-5293
Preparer Fax
406-628-5390
Prepared Date
2013-10-24 00:00:00
Authorizer Name
J*** T******
Authorizer Telephone
406-628-5200
Authorizer Title
President Cenex Pipeline
Authorizer Email
J***********@c*****.com
Narrative
On july 9, 2013, cenex pipeline was delivering product into the glendive terminal with the balance pumping to minot, nd at a rate of approximately 1100 barrels per hour. At approximately 3:02 p.M. Mdt, the cenex pipeline controller noticed a significant pressure drop at the discharge of glendive terminal and arnegard station. The controller began to shut down the 8 inch diameter pipeline segment between glendive and minot as a result of an unexplained pressure drop and had the pipeline shutdown and rov's closed by 3:05 and 25 seconds. At approximately 3:11 p.M., a representative of the excavator phoned the control center to report that their company may have hit the pipeline during excavation and believe that it is damaged. The excavator reported the approximate location of the release in the area between alexander and arnegard in section 26 and 27. The puncture occurred near cenex pipeline mile post 81, and a photograph of the damaged pipe is included in exhibit section 7. Cenex pipeline estimates that 870 barrels of gasoline was released at the site with approximately 38 barrels of free product being recovered. The released product did not ignite, did not reach any surface water, and there were no reported injuries or fatalities as a result of this release. The cause of this damage was determined to be excavator failure to notify the one call center of a change in location of the excavation. The excavator rerouted the excavation 373' away from the original planned excavation route, that was previously marked by cenex pipeline and hydro excavated at the planned crossing location, in coordination with the excavator. The reroute location was within view of the existing cenex pipeline markings at the planned excavation location. Upon deciding to reroute the excavation, the excavator failed to contact nd one call to request a new locate nor did they contact cenex pipeline to provide notification of the change in route. 1353 tons of contaminated soil were transported to ihd solids management, llc - williston, nd for disposal.
Report Received Date 2013-08-07 00:00:00
Iyear 2013
Report Number 20130269
Supplemental Number 18656
Report Type Supplemental Final
Operator Id 2170 PHMSA Enforcement
Name Cenex Pipeline Llc
Operator Street Address 803 Hwy 212 S (Po Box 909)
Operator City Name Laurel
Operator State Abbreviation MT
Operator Postal Code 59044
Local Datetime 2013-07-09 15:02:00
Location Latitude 47.7826 Google Maps OpenStreetMap
Location Longitude -103.56694 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 870
Recovered Bbls 820
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2013-07-09 15:02:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-07-09 15:05:00
Restart Datetime 2013-07-12 17:45:00
On Site Datetime 2013-07-09 17:15:00
Nrc Rpt Datetime 2013-07-09 15:28:00
Nrc Rpt Num 1053247 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name Glendive To Minot 8"
Segment Name Glendive To Minot 8"
Onshore State Abbreviation Nd
Onshore Postal Code 58835
Onshore City Name Nearest City Was Arnegard, Nd
Onshore County Name Mckenzie
Designated Location Milepost/valve Station
Designated Name 81
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.188
Pipe Smys 46000
Pipe Specification Api 5l X46
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Cal-Metal
Pipe Coating Type Coal Tar
Installation Year 1960
Manufactured Year 1960
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 7
Puncture Circum 9
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 15000
Est Cost Gas Released 110000
Est Cost Prop Damage 30000
Est Cost Emergency 150000
Est Cost Environmental 220000
Est Cost Other 50000
Est Cost Other Details Continued Monitoring.
Prpty 575000
Accident Psig 500
Mop Psig 1135
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 453244
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind Yes
Invest No Schedule Ind Details It Was Determined That Controller Action Did Not Contribute To This Incident. The Controller Followed Procedures And Responded Appropriately And Promptly To The Incident, Therefore There Was No Cause To Further Investigate Fatigue.
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Water
One Call Notified Ind Yes
One Call Ticket Num 13093161
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 75
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name M******* S*****
Preparer Title Dot Compliance Coordinator
Preparer Email M**************@c*****.com
Preparer Telephone 406-628-5293
Preparer Fax 406-628-5390
Prepared Date 2013-10-24 00:00:00
Authorizer Name J*** T******
Authorizer Telephone 406-628-5200
Authorizer Title President Cenex Pipeline
Authorizer Email J***********@c*****.com
Narrative On july 9, 2013, cenex pipeline was delivering product into the glendive terminal with the balance pumping to minot, nd at a rate of approximately 1100 barrels per hour. At approximately 3:02 p.M. Mdt, the cenex pipeline controller noticed a significant pressure drop at the discharge of glendive terminal and arnegard station. The controller began to shut down the 8 inch diameter pipeline segment between glendive and minot as a result of an unexplained pressure drop and had the pipeline shutdown and rov's closed by 3:05 and 25 seconds. At approximately 3:11 p.M., a representative of the excavator phoned the control center to report that their company may have hit the pipeline during excavation and believe that it is damaged. The excavator reported the approximate location of the release in the area between alexander and arnegard in section 26 and 27. The puncture occurred near cenex pipeline mile post 81, and a photograph of the damaged pipe is included in exhibit section 7. Cenex pipeline estimates that 870 barrels of gasoline was released at the site with approximately 38 barrels of free product being recovered. The released product did not ignite, did not reach any surface water, and there were no reported injuries or fatalities as a result of this release. The cause of this damage was determined to be excavator failure to notify the one call center of a change in location of the excavation. The excavator rerouted the excavation 373' away from the original planned excavation route, that was previously marked by cenex pipeline and hydro excavated at the planned crossing location, in coordination with the excavator. The reroute location was within view of the existing cenex pipeline markings at the planned excavation location. Upon deciding to reroute the excavation, the excavator failed to contact nd one call to request a new locate nor did they contact cenex pipeline to provide notification of the change in route. 1353 tons of contaminated soil were transported to ihd solids management, llc - williston, nd for disposal.

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