HL incident on 2013-07-03 — TX

Operator
Phillips 66 Pipeline Llc
Cause
Natural Force Damage
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500,000
Incident datetime
2013-07-03 07:30
Report number
Location
TX
Narrative
The local area supervisor in billings recieved a call from the control center at 5:45 pm mst on 07/02/2013, regarding a pressure differential downstream of a block valve at ~mp 22 on sm01 seminoe mainline and the line had been shut down. The area supervisor, a technician and a pipeliner headed to the approximate location to investigate and the line flyer was released for assistance nothing was found on 07/02/2013. On 07/03/13 crews continued to investigate and the leak was found by the line flyer. Upon this discovery, operations and contract crews immediately headed to the site and began work. Line was stress releived for about 4000 feet and repairs were made to the line. Additional safety items were performed as requested by PHMSA on the line and started back up on 07/13/2013. Pressure downstream of the valve is ~25 psi and upstream is ~325 psi. Mp 22 is 20 miles south of billings and technically within crow reservation boundaries.
Detailed record list
Report Received Date
2013-08-01 00:00:00
Iyear
2013
Report Number
20130263
Supplemental Number
18912
Report Type
Supplemental Final
Operator Id
Name
Phillips 66 Pipeline Llc
Operator Street Address
2331 Citywest Blvd
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2013-07-02 17:25:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
411
Recovered Bbls
11
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2013-07-03 07:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-07-02 17:26:00
Restart Datetime
2013-07-13 09:00:00
On Site Datetime
2013-07-03 08:00:00
Nrc Rpt Datetime
2013-07-03 08:42:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Seminoe Pipe Line
Segment Name
Sm-01
Onshore State Abbreviation
Mt
Onshore Postal Code
59075
Onshore City Name
St. Xavier
Onshore County Name
Bighorn
Designated Location
Milepost/valve Station
Designated Name
Mp 54.2
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
30
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
8.625
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Kaiser Steel
Pipe Coating Type
Coal Tar
Installation Year
1963
Manufactured Year
1963
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Width
1
Rupture Length
28
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
10000
Est Cost Gas Released
60935
Est Cost Prop Damage
1500000
Est Cost Emergency
0
Est Cost Environmental
414852
Est Cost Other
0
Prpty
1985787
Accident Psig
1295
Mop Psig
1632
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
87965
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A sudden pressure drop was discovered by the controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Earth Movement, Not Due To Heavy Rains/floods
Natural Force Type
Earth Movement, Not Due To Heavy Rains/floods
Earth Subtype
Landslide
Nf Extreme Weather Ind
No
Preparer Name
M****** J* D******
Preparer Title
Dot Coordinator
Preparer Email
M****************@p**.com
Preparer Telephone
406.855.6963
Preparer Fax
406.255.5734
Prepared Date
2014-01-10 00:00:00
Authorizer Name
T*** L* T*****
Authorizer Telephone
832.765.1636
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
T************@p**.com
Narrative
The local area supervisor in billings recieved a call from the control center at 5:45 pm mst on 07/02/2013, regarding a pressure differential downstream of a block valve at ~mp 22 on sm01 seminoe mainline and the line had been shut down. The area supervisor, a technician and a pipeliner headed to the approximate location to investigate and the line flyer was released for assistance nothing was found on 07/02/2013. On 07/03/13 crews continued to investigate and the leak was found by the line flyer. Upon this discovery, operations and contract crews immediately headed to the site and began work. Line was stress releived for about 4000 feet and repairs were made to the line. Additional safety items were performed as requested by PHMSA on the line and started back up on 07/13/2013. Pressure downstream of the valve is ~25 psi and upstream is ~325 psi. Mp 22 is 20 miles south of billings and technically within crow reservation boundaries.
Report Received Date 2013-08-01 00:00:00
Iyear 2013
Report Number 20130263
Supplemental Number 18912
Report Type Supplemental Final
Operator Id 31684 PHMSA Enforcement
Name Phillips 66 Pipeline Llc
Operator Street Address 2331 Citywest Blvd
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2013-07-02 17:25:00
Location Latitude 45.250322 Google Maps OpenStreetMap
Location Longitude -107.701801 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 411
Recovered Bbls 11
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2013-07-03 07:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-07-02 17:26:00
Restart Datetime 2013-07-13 09:00:00
On Site Datetime 2013-07-03 08:00:00
Nrc Rpt Datetime 2013-07-03 08:42:00
Nrc Rpt Num 105628 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name Seminoe Pipe Line
Segment Name Sm-01
Onshore State Abbreviation Mt
Onshore Postal Code 59075
Onshore City Name St. Xavier
Onshore County Name Bighorn
Designated Location Milepost/valve Station
Designated Name Mp 54.2
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 30
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 8.625
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Kaiser Steel
Pipe Coating Type Coal Tar
Installation Year 1963
Manufactured Year 1963
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Width 1
Rupture Length 28
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 10000
Est Cost Gas Released 60935
Est Cost Prop Damage 1500000
Est Cost Emergency 0
Est Cost Environmental 414852
Est Cost Other 0
Prpty 1985787
Accident Psig 1295
Mop Psig 1632
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 87965
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A sudden pressure drop was discovered by the controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Earth Movement, Not Due To Heavy Rains/floods
Natural Force Type Earth Movement, Not Due To Heavy Rains/floods
Earth Subtype Landslide
Nf Extreme Weather Ind No
Preparer Name M****** J* D******
Preparer Title Dot Coordinator
Preparer Email M****************@p**.com
Preparer Telephone 406.855.6963
Preparer Fax 406.255.5734
Prepared Date 2014-01-10 00:00:00
Authorizer Name T*** L* T*****
Authorizer Telephone 832.765.1636
Authorizer Title Regulatory Compliance Manager
Authorizer Email T************@p**.com
Narrative The local area supervisor in billings recieved a call from the control center at 5:45 pm mst on 07/02/2013, regarding a pressure differential downstream of a block valve at ~mp 22 on sm01 seminoe mainline and the line had been shut down. The area supervisor, a technician and a pipeliner headed to the approximate location to investigate and the line flyer was released for assistance nothing was found on 07/02/2013. On 07/03/13 crews continued to investigate and the leak was found by the line flyer. Upon this discovery, operations and contract crews immediately headed to the site and began work. Line was stress releived for about 4000 feet and repairs were made to the line. Additional safety items were performed as requested by PHMSA on the line and started back up on 07/13/2013. Pressure downstream of the valve is ~25 psi and upstream is ~325 psi. Mp 22 is 20 miles south of billings and technically within crow reservation boundaries.

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