Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2013-07-11 — KS
Operator
Jayhawk Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$700
Incident datetime
2013-07-11 11:00
Report number
Location
KS
Narrative
When the station operator arrived at the mcpherson station he discovered that the booster pump seal had been leaking. The emergency response plan was initiated and cleanup was performed. Nrc, kdhe, and PHMSA was notified. The seal around the pump shaft split which resulted in the release. The seal was replaced and the pump checked out and determined operational. Snapchart from incident review attached.
Detailed record list
Report Received Date
2013-07-30 00:00:00
Iyear
2013
Report Number
20130260
Supplemental Number
18775
Report Type
Supplemental Final
Operator Id
9175
Name
Jayhawk Pipeline Llc
Operator Street Address
2000 S. Main
Operator City Name
Mcpherson
Operator State Abbreviation
KS
Operator Postal Code
67460
Local Datetime
2013-07-11 11:00:00
Location Latitude
38.3362
Location Longitude
-97.67782
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.9
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pump Was Already Down When Discovered.
Nrc Rpt Datetime
2013-07-11 11:35:00
Nrc Rpt Num
1053461
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Mcpherson Station
Onshore State Abbreviation
Ks
Onshore Postal Code
67460
Onshore City Name
Mcpherson
Onshore County Name
Mcpherson
Designated Location
Milepost/valve Station
Designated Name
Mp1
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
700
Est Cost Emergency
1000
Est Cost Environmental
5800
Est Cost Other
2400
Est Cost Other Details
Future Tap Root Investigation
Prpty
10000
Pipeline Function
< 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
J**** W*****
Preparer Title
Regulatory Compliance Manager
Preparer Email
J******@n***.coop
Preparer Telephone
6202419253
Prepared Date
2013-11-26 00:00:00
Authorizer Name
J**** W*****
Authorizer Telephone
6202419253
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
J******@n***.coop
Narrative
When the station operator arrived at the mcpherson station he discovered that the booster pump seal had been leaking. The emergency response plan was initiated and cleanup was performed. Nrc, kdhe, and PHMSA was notified. The seal around the pump shaft split which resulted in the release. The seal was replaced and the pump checked out and determined operational. Snapchart from incident review attached.
| Report Received Date | 2013-07-30 00:00:00 |
|---|---|
| Iyear | 2013 |
| Report Number | 20130260 |
| Supplemental Number | 18775 |
| Report Type | Supplemental Final |
| Operator Id | 9175 PHMSA Enforcement |
| Name | Jayhawk Pipeline Llc |
| Operator Street Address | 2000 S. Main |
| Operator City Name | Mcpherson |
| Operator State Abbreviation | KS |
| Operator Postal Code | 67460 |
| Local Datetime | 2013-07-11 11:00:00 |
| Location Latitude | 38.3362 Google Maps OpenStreetMap |
| Location Longitude | -97.67782 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.9 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Pump Was Already Down When Discovered. |
| Nrc Rpt Datetime | 2013-07-11 11:35:00 |
| Nrc Rpt Num | 1053461 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Mcpherson Station |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 67460 |
| Onshore City Name | Mcpherson |
| Onshore County Name | Mcpherson |
| Designated Location | Milepost/valve Station |
| Designated Name | Mp1 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Pump |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 100 |
| Est Cost Prop Damage | 700 |
| Est Cost Emergency | 1000 |
| Est Cost Environmental | 5800 |
| Est Cost Other | 2400 |
| Est Cost Other Details | Future Tap Root Investigation |
| Prpty | 10000 |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Preparer Name | J**** W***** |
| Preparer Title | Regulatory Compliance Manager |
| Preparer Email | J******@n***.coop |
| Preparer Telephone | 6202419253 |
| Prepared Date | 2013-11-26 00:00:00 |
| Authorizer Name | J**** W***** |
| Authorizer Telephone | 6202419253 |
| Authorizer Title | Regulatory Compliance Manager |
| Authorizer Email | J******@n***.coop |
| Narrative | When the station operator arrived at the mcpherson station he discovered that the booster pump seal had been leaking. The emergency response plan was initiated and cleanup was performed. Nrc, kdhe, and PHMSA was notified. The seal around the pump shaft split which resulted in the release. The seal was replaced and the pump checked out and determined operational. Snapchart from incident review attached. |
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