HL incident on 2013-07-01 — OK

Operator
Magellan Ammonia Pipeline, L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$108,000
Incident datetime
2013-07-01 17:20
Report number
Location
OK
Narrative
Aerial patrol pilot identified a potential dead spot of vegetation and notified magellan personnel who investigated and determined a release had occurred. The site was excavated and a buried check valve was found to be leaking. The line was isolated and the valve lid was removed, whereupon a damaged o-ring gasket was found to be the source of the release. A new o-ring gasket was installed and the head bolts were torqued to manufacturer's specifications. Approximately 100 cubic yards of impacted soil was remediated in accordance with state and company standards.
Detailed record list
Report Received Date
2013-07-30 00:00:00
Iyear
2013
Report Number
20130259
Supplemental Number
19214
Report Type
Supplemental Final
Operator Id
Name
Magellan Ammonia Pipeline, L.p.
Operator Street Address
One Williams Center, Otc-9 P.o. Box 22186
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2013-07-01 17:20:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
5
Intentional Release Bbls
5.95
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Operator Employee
Incident Identified Datetime
2013-07-01 17:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Already Down Due To A Pinhole Release At Mp 107 Discovered Earlier
On Site Datetime
2013-07-01 19:20:00
Nrc Rpt Datetime
2013-07-01 17:58:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Pipe Fac Name
Pocahontas To Luverne 6-Inch Line
Segment Name
Line Segment Id 504
Onshore State Abbreviation
Ia
Onshore Postal Code
50520
Onshore City Name
Bradgate
Onshore County Name
Humboldt
Designated Location
Milepost/valve Station
Designated Name
104.7
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Check
Valve Manufacturer
Wheatley
Installation Year
2011
Manufactured Year
2011
Material Involved
Material Other Than Carbon Steel
Material Details
Neoprene
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
2500
Est Cost Gas Released
403
Est Cost Prop Damage
108000
Est Cost Emergency
43000
Est Cost Environmental
35000
Est Cost Other
0
Prpty
188903
Accident Psig
430
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
39117
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was the result of a malfunction in a check valve. It was subsequently determined that neither the control room nor the controller on duty caused or contributed to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
O-Ring Gasket Was Damaged From Undetermined Causes
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2014-04-03 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Aerial patrol pilot identified a potential dead spot of vegetation and notified magellan personnel who investigated and determined a release had occurred. The site was excavated and a buried check valve was found to be leaking. The line was isolated and the valve lid was removed, whereupon a damaged o-ring gasket was found to be the source of the release. A new o-ring gasket was installed and the head bolts were torqued to manufacturer's specifications. Approximately 100 cubic yards of impacted soil was remediated in accordance with state and company standards.
Report Received Date 2013-07-30 00:00:00
Iyear 2013
Report Number 20130259
Supplemental Number 19214
Report Type Supplemental Final
Operator Id 12105 PHMSA Enforcement
Name Magellan Ammonia Pipeline, L.p.
Operator Street Address One Williams Center, Otc-9 P.o. Box 22186
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2013-07-01 17:20:00
Location Latitude 42.79375 Google Maps OpenStreetMap
Location Longitude -94.40176 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 5
Intentional Release Bbls 5.95
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Operator Employee
Incident Identified Datetime 2013-07-01 17:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Already Down Due To A Pinhole Release At Mp 107 Discovered Earlier
On Site Datetime 2013-07-01 19:20:00
Nrc Rpt Datetime 2013-07-01 17:58:00
Nrc Rpt Num 1052346 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Pipe Fac Name Pocahontas To Luverne 6-Inch Line
Segment Name Line Segment Id 504
Onshore State Abbreviation Ia
Onshore Postal Code 50520
Onshore City Name Bradgate
Onshore County Name Humboldt
Designated Location Milepost/valve Station
Designated Name 104.7
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Check
Valve Manufacturer Wheatley
Installation Year 2011
Manufactured Year 2011
Material Involved Material Other Than Carbon Steel
Material Details Neoprene
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 2500
Est Cost Gas Released 403
Est Cost Prop Damage 108000
Est Cost Emergency 43000
Est Cost Environmental 35000
Est Cost Other 0
Prpty 188903
Accident Psig 430
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 39117
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was the result of a malfunction in a check valve. It was subsequently determined that neither the control room nor the controller on duty caused or contributed to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Check Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details O-Ring Gasket Was Damaged From Undetermined Causes
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7377
Prepared Date 2014-04-03 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative Aerial patrol pilot identified a potential dead spot of vegetation and notified magellan personnel who investigated and determined a release had occurred. The site was excavated and a buried check valve was found to be leaking. The line was isolated and the valve lid was removed, whereupon a damaged o-ring gasket was found to be the source of the release. A new o-ring gasket was installed and the head bolts were torqued to manufacturer's specifications. Approximately 100 cubic yards of impacted soil was remediated in accordance with state and company standards.

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