HL incident on 2013-06-26 — TX

Operator
Valero Terminaling And Distribution Company
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-06-26 12:10
Report number
Location
TX
Narrative
During pipeline startup the third party receiving ultra-low sulphur diesel failed to open the valve to the receiving tank. The control valve and the thermal relief valves on meter run at the end of the pipeline were set at the same pressure. The thermal relief valves relieved into a sump. Product was released through the sump vent as the line packed during startup. Valero has since lowered the control valve setting.
Detailed record list
Report Received Date
2013-07-26 00:00:00
Iyear
2013
Report Number
20130256
Supplemental Number
18437
Report Type
Supplemental Final
Operator Id
Name
Valero Terminaling And Distribution Company
Operator Street Address
One Valero Way
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78249
Local Datetime
2013-06-26 12:10:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
21
Recovered Bbls
21
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-06-26 12:10:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
On Site Datetime
2013-06-26 12:10:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Vtdc Par To Teppco 12-10 Products - 10&12"
Segment Name
Vtdc Par To Teppco 12-10 Products - 10&12"
Onshore State Abbreviation
Tx
Onshore Postal Code
77705
Onshore City Name
Beaumont
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Oti Meter Sta
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Sump
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Unknown
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
No
Other Pop Ind
Yes
Other Pop Yes No
No
Usa Drinking Ind
Yes
Usa Drinking Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
13000
Est Cost Other
0
Prpty
13000
Accident Psig
275
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Other Ind
Yes
Operation Related Details
Control Valve And Thermal Relief Valves Set At Same Setting.
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
J**** T******
Preparer Title
Lead Regulatory Compliance Specialist
Preparer Email
J************@v*****.com
Preparer Telephone
2103455145
Preparer Fax
2103706235
Prepared Date
2013-08-09 00:00:00
Authorizer Name
J**** T******
Authorizer Telephone
2103455145
Authorizer Title
Lead Regulatory Compliance Specialist
Authorizer Email
J************@v*****.com
Narrative
During pipeline startup the third party receiving ultra-low sulphur diesel failed to open the valve to the receiving tank. The control valve and the thermal relief valves on meter run at the end of the pipeline were set at the same pressure. The thermal relief valves relieved into a sump. Product was released through the sump vent as the line packed during startup. Valero has since lowered the control valve setting.
Report Received Date 2013-07-26 00:00:00
Iyear 2013
Report Number 20130256
Supplemental Number 18437
Report Type Supplemental Final
Operator Id 4430 PHMSA Enforcement
Name Valero Terminaling And Distribution Company
Operator Street Address One Valero Way
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78249
Local Datetime 2013-06-26 12:10:00
Location Latitude 30.0095 Google Maps OpenStreetMap
Location Longitude -94.0594 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 21
Recovered Bbls 21
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2013-06-26 12:10:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
On Site Datetime 2013-06-26 12:10:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Vtdc Par To Teppco 12-10 Products - 10&12"
Segment Name Vtdc Par To Teppco 12-10 Products - 10&12"
Onshore State Abbreviation Tx
Onshore Postal Code 77705
Onshore City Name Beaumont
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name Oti Meter Sta
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Sump
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Unknown
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No No
Other Pop Ind Yes
Other Pop Yes No No
Usa Drinking Ind Yes
Usa Drinking Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 13000
Est Cost Other 0
Prpty 13000
Accident Psig 275
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Other Ind Yes
Operation Related Details Control Valve And Thermal Relief Valves Set At Same Setting.
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name J**** T******
Preparer Title Lead Regulatory Compliance Specialist
Preparer Email J************@v*****.com
Preparer Telephone 2103455145
Preparer Fax 2103706235
Prepared Date 2013-08-09 00:00:00
Authorizer Name J**** T******
Authorizer Telephone 2103455145
Authorizer Title Lead Regulatory Compliance Specialist
Authorizer Email J************@v*****.com
Narrative During pipeline startup the third party receiving ultra-low sulphur diesel failed to open the valve to the receiving tank. The control valve and the thermal relief valves on meter run at the end of the pipeline were set at the same pressure. The thermal relief valves relieved into a sump. Product was released through the sump vent as the line packed during startup. Valero has since lowered the control valve setting.

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