HL incident on 2013-06-16 — OH

Operator
Marathon Pipe Line Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-06-16 09:30
Report number
Location
OH
Narrative
Pig trap door was sealed but the seal did not hold product leaked into secondary containment. The pig trap was cleaned of any excess product and the door was re-sealed.
Detailed record list
Report Received Date
2013-07-03 00:00:00
Iyear
2013
Report Number
20130240
Supplemental Number
19182
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2013-06-16 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2013-06-16 09:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
On Site Datetime
2013-06-16 09:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Canton - East Sparta 6" Products
Segment Name
Canton - East Sparta #1-6"
Onshore State Abbreviation
Oh
Onshore Postal Code
44626
Onshore City Name
East Sparta
Onshore County Name
Stark
Designated Location
Milepost/valve Station
Designated Name
443+34
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
23
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
23
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
R**** S********
Preparer Title
Hes Regulatory Compliance Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2014-03-27 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
Pig trap door was sealed but the seal did not hold product leaked into secondary containment. The pig trap was cleaned of any excess product and the door was re-sealed.
Report Received Date 2013-07-03 00:00:00
Iyear 2013
Report Number 20130240
Supplemental Number 19182
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2013-06-16 09:30:00
Location Latitude 40.676504 Google Maps OpenStreetMap
Location Longitude -81.347693 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.2
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2013-06-16 09:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
On Site Datetime 2013-06-16 09:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Canton - East Sparta 6" Products
Segment Name Canton - East Sparta #1-6"
Onshore State Abbreviation Oh
Onshore Postal Code 44626
Onshore City Name East Sparta
Onshore County Name Stark
Designated Location Milepost/valve Station
Designated Name 443+34
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 23
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 23
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Preparer Name R**** S********
Preparer Title Hes Regulatory Compliance Professional
Preparer Email R**********@m****************.com
Preparer Telephone 419-421-2121
Prepared Date 2014-03-27 00:00:00
Authorizer Name R****** B*****
Authorizer Telephone 419-421-2121
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative Pig trap door was sealed but the seal did not hold product leaked into secondary containment. The pig trap was cleaned of any excess product and the door was re-sealed.

All rights reserved. Copyright © by ClearPHMSA