HL incident on 2013-05-31 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$150,000
Incident datetime
2013-05-31 11:20
Report number
Location
TX
Narrative
On april 17, 2013, enterprise installed a split tee for the purpose of establishing an interconnect to another pipeline. On may 31 at 11:20 am while hot tapping the split tee, a contractor noticed a leak from the split tee circumferential weld as soon as the pilot bit penetrated the inner surface of the carrier pipe. The contractor immediately shut down their equipment and notified an on-site company employee who stopped the work and evacuated personnel from the leak site. The company employee notified pl control who shut down the pipeline at 11:30 am. The line segment was initially isolated at mocane station (south of the leak site) and the line pressure was reduced to approximately 300 psig. The leak site was then isolated by closing the mainline block valve approximately 11 miles north of mocane station. On june 1, work was initiated to install stopples on both sides of the leak. On june 4, the stopples were set and leak site was isolated, then blown down. On june 5, a cut out was made and replacement pipe was installed along with a new tee. On june 6, the stopples were retracted and the pipeline was purged to allow the line to return to service. Metallurgical analysis of the failure segment identified a crack in the circumferential weld of the split tee where the leak occurred. Material analysis of the weld material identified the filler material contained more chromium than appropriate. Enterprise believes that the welding procedure is in compliance with applicable regulations and is technically sound, however recognizes that the procedure can be improved to provide additional clarity when selecting welding consumables for certain jobs and is taking action to provide that clarification.
Detailed record list
Report Received Date
2013-06-28 00:00:00
Iyear
2013
Report Number
20130230
Supplemental Number
18621
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2013-05-31 11:20:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Y-Grade
Unintentional Release Bbls
200
Intentional Release Bbls
14.5
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2013-05-31 11:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-05-31 11:30:00
Restart Datetime
2013-06-06 14:34:00
On Site Datetime
2013-05-31 11:20:00
Nrc Rpt Datetime
2013-05-31 12:37:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
South Leg Brown Line
Segment Name
Lid 7465
Onshore State Abbreviation
Ok
Onshore Postal Code
73938
Onshore City Name
Forgan
Onshore County Name
Beaver
Designated Location
Milepost/valve Station
Designated Name
Milepost 341
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Weld Subtype
Fillet Weld
Installation Year
2013
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
7000
Est Cost Prop Damage
150000
Est Cost Emergency
150000
Est Cost Environmental
0
Est Cost Other
18000
Est Cost Other Details
Metallurgical Analysis Of Failure Segment.
Prpty
325000
Accident Psig
820
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
59400
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
2
Num Employees Failed
0
Num Contractors Tested
2
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Welding Procedures And Pre-Assessment Letter Do Not Specify The Type Of Welding Electrodes To Utilizer Per Application.
Related Other Ind
Yes
Operation Related Details
Welding Procedures And Pre-Assessment Letter Do Not Specify The Type Of Welding Electrodes To Utilizer Per Application.
Category Type
Right-Of-Way Activities
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
N*** T*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
N*******@e****.com
Preparer Telephone
713-381-2493
Prepared Date
2013-09-25 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
N*******@e****.com
Narrative
On april 17, 2013, enterprise installed a split tee for the purpose of establishing an interconnect to another pipeline. On may 31 at 11:20 am while hot tapping the split tee, a contractor noticed a leak from the split tee circumferential weld as soon as the pilot bit penetrated the inner surface of the carrier pipe. The contractor immediately shut down their equipment and notified an on-site company employee who stopped the work and evacuated personnel from the leak site. The company employee notified pl control who shut down the pipeline at 11:30 am. The line segment was initially isolated at mocane station (south of the leak site) and the line pressure was reduced to approximately 300 psig. The leak site was then isolated by closing the mainline block valve approximately 11 miles north of mocane station. On june 1, work was initiated to install stopples on both sides of the leak. On june 4, the stopples were set and leak site was isolated, then blown down. On june 5, a cut out was made and replacement pipe was installed along with a new tee. On june 6, the stopples were retracted and the pipeline was purged to allow the line to return to service. Metallurgical analysis of the failure segment identified a crack in the circumferential weld of the split tee where the leak occurred. Material analysis of the weld material identified the filler material contained more chromium than appropriate. Enterprise believes that the welding procedure is in compliance with applicable regulations and is technically sound, however recognizes that the procedure can be improved to provide additional clarity when selecting welding consumables for certain jobs and is taking action to provide that clarification.
Report Received Date 2013-06-28 00:00:00
Iyear 2013
Report Number 20130230
Supplemental Number 18621
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2013-05-31 11:20:00
Location Latitude 36.947219 Google Maps OpenStreetMap
Location Longitude -100.293152 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Y-Grade
Unintentional Release Bbls 200
Intentional Release Bbls 14.5
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2013-05-31 11:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-05-31 11:30:00
Restart Datetime 2013-06-06 14:34:00
On Site Datetime 2013-05-31 11:20:00
Nrc Rpt Datetime 2013-05-31 12:37:00
Nrc Rpt Num 1048859 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name South Leg Brown Line
Segment Name Lid 7465
Onshore State Abbreviation Ok
Onshore Postal Code 73938
Onshore City Name Forgan
Onshore County Name Beaver
Designated Location Milepost/valve Station
Designated Name Milepost 341
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Weld Subtype Fillet Weld
Installation Year 2013
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 7000
Est Cost Prop Damage 150000
Est Cost Emergency 150000
Est Cost Environmental 0
Est Cost Other 18000
Est Cost Other Details Metallurgical Analysis Of Failure Segment.
Prpty 325000
Accident Psig 820
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 59400
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 2
Num Employees Failed 0
Num Contractors Tested 2
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Welding Procedures And Pre-Assessment Letter Do Not Specify The Type Of Welding Electrodes To Utilizer Per Application.
Related Other Ind Yes
Operation Related Details Welding Procedures And Pre-Assessment Letter Do Not Specify The Type Of Welding Electrodes To Utilizer Per Application.
Category Type Right-Of-Way Activities
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name N*** T*****
Preparer Title Pipeline Compliance Engineer
Preparer Email N*******@e****.com
Preparer Telephone 713-381-2493
Prepared Date 2013-09-25 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 713-381-2493
Authorizer Title Pipeline Compliance Engineer
Authorizer Email N*******@e****.com
Narrative On april 17, 2013, enterprise installed a split tee for the purpose of establishing an interconnect to another pipeline. On may 31 at 11:20 am while hot tapping the split tee, a contractor noticed a leak from the split tee circumferential weld as soon as the pilot bit penetrated the inner surface of the carrier pipe. The contractor immediately shut down their equipment and notified an on-site company employee who stopped the work and evacuated personnel from the leak site. The company employee notified pl control who shut down the pipeline at 11:30 am. The line segment was initially isolated at mocane station (south of the leak site) and the line pressure was reduced to approximately 300 psig. The leak site was then isolated by closing the mainline block valve approximately 11 miles north of mocane station. On june 1, work was initiated to install stopples on both sides of the leak. On june 4, the stopples were set and leak site was isolated, then blown down. On june 5, a cut out was made and replacement pipe was installed along with a new tee. On june 6, the stopples were retracted and the pipeline was purged to allow the line to return to service. Metallurgical analysis of the failure segment identified a crack in the circumferential weld of the split tee where the leak occurred. Material analysis of the weld material identified the filler material contained more chromium than appropriate. Enterprise believes that the welding procedure is in compliance with applicable regulations and is technically sound, however recognizes that the procedure can be improved to provide additional clarity when selecting welding consumables for certain jobs and is taking action to provide that clarification.

All rights reserved. Copyright © by ClearPHMSA