HL incident on 2013-06-01 — WY

Operator
Belle Fourche Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2013-06-01 13:00
Report number
Location
WY
Narrative
Pump seal became disengaged from the pump and allowed the product to flow freely out of the pump between the shaft and the casing. Operator personnel observed the leak and had the pump shut down. Vac trucks were brought in to clean up free standing oil and contaminated soil was excavated and collected for proper disposal. Pipeline was restarted the following day after cleanup was completed.
Detailed record list
Report Received Date
2013-06-28 00:00:00
Iyear
2013
Report Number
20130229
Supplemental Number
18237
Report Type
Original Final
Operator Id
Name
Belle Fourche Pipeline Co
Operator Street Address
455 N Poplar St.
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82602
Local Datetime
2013-06-01 12:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
135
Recovered Bbls
130
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2013-06-01 13:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2013-06-01 13:15:00
Restart Datetime
2013-06-02 11:00:00
On Site Datetime
2013-06-01 14:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Osage 8"
Onshore State Abbreviation
Wy
Onshore Postal Code
82723
Onshore City Name
Osage
Onshore County Name
Weston
Designated Location
Milepost/valve Station
Designated Name
0
Federal
Yes
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Mechanical Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
5000
Est Cost Other
0
Prpty
5500
Accident Psig
143
Mop Psig
1000
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Seal leaks are not monitored by the control room for this pump and are not typically noticed by a controller at the low pressure and flow rate at which this pipeline operates. Pressure trends were reviewed to see if there was anything out of the ordinary that may have tipped off a controller and nothing was noted.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Additional Defect Ind
Yes
Preparer Name
K** D*********
Preparer Title
Dot Compliance Supervisor
Preparer Email
K*************@t******.com
Preparer Telephone
307-266-0275
Prepared Date
2013-06-28 00:00:00
Authorizer Name
K** D*********
Authorizer Telephone
307-266-0275
Authorizer Title
Dot Compliance Supervisor
Authorizer Email
K*************@t******.com
Narrative
Pump seal became disengaged from the pump and allowed the product to flow freely out of the pump between the shaft and the casing. Operator personnel observed the leak and had the pump shut down. Vac trucks were brought in to clean up free standing oil and contaminated soil was excavated and collected for proper disposal. Pipeline was restarted the following day after cleanup was completed.
Report Received Date 2013-06-28 00:00:00
Iyear 2013
Report Number 20130229
Supplemental Number 18237
Report Type Original Final
Operator Id 1248 PHMSA Enforcement
Name Belle Fourche Pipeline Co
Operator Street Address 455 N Poplar St.
Operator City Name Casper
Operator State Abbreviation WY
Operator Postal Code 82602
Local Datetime 2013-06-01 12:30:00
Location Latitude 43.992624 Google Maps OpenStreetMap
Location Longitude -104.388373 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 135
Recovered Bbls 130
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2013-06-01 13:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2013-06-01 13:15:00
Restart Datetime 2013-06-02 11:00:00
On Site Datetime 2013-06-01 14:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Osage 8"
Onshore State Abbreviation Wy
Onshore Postal Code 82723
Onshore City Name Osage
Onshore County Name Weston
Designated Location Milepost/valve Station
Designated Name 0
Federal Yes
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Mechanical Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 5000
Est Cost Other 0
Prpty 5500
Accident Psig 143
Mop Psig 1000
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Seal leaks are not monitored by the control room for this pump and are not typically noticed by a controller at the low pressure and flow rate at which this pipeline operates. Pressure trends were reviewed to see if there was anything out of the ordinary that may have tipped off a controller and nothing was noted.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Additional Defect Ind Yes
Preparer Name K** D*********
Preparer Title Dot Compliance Supervisor
Preparer Email K*************@t******.com
Preparer Telephone 307-266-0275
Prepared Date 2013-06-28 00:00:00
Authorizer Name K** D*********
Authorizer Telephone 307-266-0275
Authorizer Title Dot Compliance Supervisor
Authorizer Email K*************@t******.com
Narrative Pump seal became disengaged from the pump and allowed the product to flow freely out of the pump between the shaft and the casing. Operator personnel observed the leak and had the pump shut down. Vac trucks were brought in to clean up free standing oil and contaminated soil was excavated and collected for proper disposal. Pipeline was restarted the following day after cleanup was completed.

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